基质酸化处理后的井况——以阿赫代布油田Mi4装置为例

U. Alameedy, A. Al-haleem, Abdulameer Almalichy
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引用次数: 2

摘要

油井的生产率可以通过确定提高油井生产率的价值以及在油井被认为表现不佳后地层损坏的可能原因或来源来提高。油井生产率可能会提高,但这种逐步提高的经济性可能会受到影响。分析皮肤效应对保护区恢复的影响是很重要的。对AD-12井的酸处理进行了评估,主要针对Mi4区;使用Stimpro增产软件的许可证在现场规模上验证实验工作,该软件被认为是规划和监测基质酸处理的最全面的工具,并利用实际数据提供更好的井反应知识,其方法代表了储层之前、期间、,在基质酸处理后,通过处理后皮肤因子,这是分析刺激处理最常用的统计数据,并且依赖于虫洞区的几何形状。参考之前对Ad-12的堆积测试,-3.97的表皮值大致等于或略大于通过使用Stimpro的酸处理模拟估计的表皮值。此外,当执行模拟器时,侵入的流体揭示了处理区内两个不同的调查深度。尽管顶层虫洞穿透深度为32英寸,但底部区域的流体侵入深度为95英寸。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Well Performance Following Matrix Acidizing Treatment: Case Study of the Mi4 Unit in Ahdeb Oil Field
The productivity of oil wells may be improved by determining the value of enhancing well productivity and the likely reasons or sources of formation damage after the well has been recognized as underperforming. Oil well productivity may be improved, but the economics of this gradual improvement may be compromised. It is important to analyze the influence of the skin effect on the recovery of the reserve.    The acid treatment evaluated for the well AD-12, primarily for the zone Mi4;  using a license of Stimpro Stimulation Software to validate the experimental work to the field scale, this software is considered the most comprehensive instrument for planning and monitoring matrix acid treatments and utilizing actual data to provide a far better knowledge of the well's reaction, with methods that represent the reality of what is happening in the reservoir before, during, and after matrix acid treatments, through the post-treatment skin factor, which is the most frequently utilized statistic for analyzing stimulation treatments and relies on the geometry of the wormholed zone. Referring to the previous buildup tests for Ad-12, the skin value of -3.97 is approximately identical to or slightly larger than the skin value estimated by the acid treatment simulation using Stimpro. Moreover, when the simulator was performed, the invading fluid revealed two distinct depths of investigation inside the treated zone. While the fluid invasion in the bottom area has invaded deeply at a distance of 95 inches despite the top layer wormhole penetrating to a depth of 32 inches.
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