在 PT.Mah Sing Indonesia 公司使用整体设备效率法安排预防性维护以提高注塑机效率Mah Sing Indonesia

David Rakes, Hasyrani Windyatri, Suhendra Suhendra
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引用次数: 0

摘要

本研究旨在评估 2023 年 1 月至 12 月生产环境中的整体设备效率 (OEE)。通过定量分析,对每月的 OEE 值进行了评估,结果显示差异显著。没有一个月达到 85% 的世界级 OEE 标准,最高值出现在 8 月(54%),最低值出现在 12 月(35%)。这一时期的平均 OEE 约为 44.67%,大大低于既定基准。造成 OEE 偏低的主要因素是可用率低,导致大量机器停机。在实施结构化的预防性维护计划后,机器停机时间从 21 540 分钟显著减少到 1 464 分钟。对成型机维护的建议包括:在生产时间以外、停产期间或生产 260 000 台之后,每周进行一次维护。对于其他机器,则建议每月、每半年或每年进行一次维护。研究得出结论,适当的预防性维护计划可以显著提高 OEE,减少机器停机时间,从而提高整体生产效率。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Scheduling Preventive Maintenance to Increase the Effectiveness of Injection Molding Machines Using the Overall Equipment Effectiveness Method at PT. Mah Sing Indonesia
This study aims to evaluate the Overall Equipment Effectiveness (OEE) in a production environment from January to December 2023. Utilizing quantitative analysis, monthly OEE values were assessed, revealing significant variations. No month achieved the World Class OEE standard of 85%, with the highest value recorded in August (54%) and the lowest in December (35%). The average OEE for the period was approximately 44.67%, substantially below the established benchmark. The primary factor contributing to the low OEE was identified as the low Availability rate, leading to significant machine downtime. Following the implementation of a structured preventive maintenance schedule, machine downtime markedly decreased from 21,540 minutes to 1,464 minutes. Recommendations for moulding machine maintenance include weekly servicing outside production hours, during production halts, or after producing 260,000 units. For other machines, monthly, semi-annual, or annual maintenance schedules are proposed. The study concludes that proper preventive maintenance scheduling can significantly enhance OEE and reduce machine downtime, thereby improving overall production efficiency.
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