处理 150 兆瓦汽轮机发电厂的重大润滑油泄漏事故

Msy Cahaya Dinda Pamungkas, Chelsi Chelsi
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摘要

本文重点介绍苏姆塞勒-5 发电厂 2 号轴承箱润滑油严重泄漏的处理情况。这台超高压蒸汽轮机自 2016 年 4 月起开始运行。2019 年和 2023 年的大修解决了导油器磨损、压盖密封间隙异常和油封磨损等问题。然而,漏油现象依然存在,需要进一步干预。整改工作包括更换导油器、调整间隙、安装额外的通风管道、在 2 号轴承箱增加纤维垫片,以减少和控制漏油。这些措施大大降低了漏油率,从满负荷运行时的约 2826 毫升/小时降至 75 毫升/小时,降幅约为 97.3%。此外,润滑油加注频率大幅降低,为工厂节省了大量成本。从安全和环境角度来看,整改措施减轻了火灾隐患,减少了润滑油的浪费,最大限度地降低了对环境的影响。对润滑油质量的定期监测进一步确保了运行的可靠性。虽然没有完全消除漏油现象,但涡轮机在漏油可控的条件下继续平稳运行。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Managing a Major Lube Oil Leak on a 150 MW Steam Turbine Power Plant
This paper focuses on the management of a major lube oil leak from bearing box No. 2 at the Sumsel-5 Power Plant. The steam turbine, a super high-pressure has been operational since April 2016. Overhauls in 2019 and 2023 addressed issues such as wear on oil deflectors, abnormal gland sealing clearances, and oil sealing wear. However, oil leakage persisted, necessitating further interventions. Rectification efforts included replacing oil deflectors, adjusting clearance, installing additional venting lines, the addition of a fiber gasket at bearing box No. 2 aimed to reduce and manage oil leakage. These measures resulted in a significant reduction in the oil leakage rate, from approximately 2826 ml/hr to 75 ml/hr during full load operation, representing a decrement of around 97.3%. Additionally, the frequency of lube oil top-ups decreased dramatically, leading to substantial cost savings for the plant. From a safety and environmental perspective, rectification measures mitigated fire hazards and reduced oil wastage, minimizing environmental impact. Regular monitoring of lubrication oil quality further ensures operational reliability. Although complete elimination of the oil leak was not achieved, the turbine continues to operate smoothly under manageable oil leakage conditions.
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