Shane T King, Maura E Eveld, Karl E Zelik, Michael Goldfarb
{"title":"导致经股置换假肢使用者跌倒的因素:假肢侧趔趄恢复反应案例系列。","authors":"Shane T King, Maura E Eveld, Karl E Zelik, Michael Goldfarb","doi":"10.1186/s12984-024-01402-0","DOIUrl":null,"url":null,"abstract":"<p><strong>Background: </strong>Falls due to stumbling are prevalent for transfemoral prosthesis users and may lead to increased injury risk. This preliminary case series analyzes the transfemoral prosthesis user stumble recovery response to highlight key deficits in current commercially-available prostheses and proposes potential interventions to improve recovery outcomes.</p><p><strong>Methods: </strong>Six transfemoral prosthesis users were perturbed on their prosthetic limb at least three times while walking on a treadmill using obstacle perturbations in early, mid and late swing. Kinematic data were collected to characterize the response, while fall rate and key kinematic recovery metrics were used to assess the quality of recovery and highlight functional deficits in current commercially-available prostheses.</p><p><strong>Results: </strong>Across all participants, 13 (54%) of the 24 trials resulted in a fall (defined as > 50% body-weight support) with all but one participant (83%) falling at least once and two participants (33%) falling every time. In contrast, in a previous study of seven young, unimpaired, non-prosthesis users using the same experimental apparatus, no falls occurred across 190 trials. For the transfemoral prosthesis users, early swing had the highest rate of falling at 64%, followed by mid-swing at 57%, and then late swing at 33%. The trend in falls was mirrored by the kinematic recovery metrics (peak trunk angle, peak trunk angular velocity, forward reach of the perturbed limb, and knee angle at ground contact). In early swing all four metrics were deficient compared to non-prosthesis user controls. In mid swing, all but trunk angular velocity were deficient. In late swing only forward reach was deficient.</p><p><strong>Conclusion: </strong>Based on the stumble recovery responses, four potential deficiencies were identified in the response of the knee prostheses: (1) insufficient resistance to stance knee flexion upon ground contact; (2) insufficient swing extension after a perturbation; (3) difficulty initiating swing flexion following a perturbation; and (4) excessive impedance against swing flexion in early swing preventing the potential utilization of the elevating strategy. Each of these issues can potentially be addressed by mechanical or mechatronic changes to prosthetic design to improve quality of recovery and reduce the likelihood a fall.</p>","PeriodicalId":16384,"journal":{"name":"Journal of NeuroEngineering and Rehabilitation","volume":null,"pages":null},"PeriodicalIF":5.2000,"publicationDate":"2024-07-13","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"https://www.ncbi.nlm.nih.gov/pmc/articles/PMC11245817/pdf/","citationCount":"0","resultStr":"{\"title\":\"Factors leading to falls in transfemoral prosthesis users: a case series of prosthesis-side stumble recovery responses.\",\"authors\":\"Shane T King, Maura E Eveld, Karl E Zelik, Michael Goldfarb\",\"doi\":\"10.1186/s12984-024-01402-0\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"<p><strong>Background: </strong>Falls due to stumbling are prevalent for transfemoral prosthesis users and may lead to increased injury risk. This preliminary case series analyzes the transfemoral prosthesis user stumble recovery response to highlight key deficits in current commercially-available prostheses and proposes potential interventions to improve recovery outcomes.</p><p><strong>Methods: </strong>Six transfemoral prosthesis users were perturbed on their prosthetic limb at least three times while walking on a treadmill using obstacle perturbations in early, mid and late swing. Kinematic data were collected to characterize the response, while fall rate and key kinematic recovery metrics were used to assess the quality of recovery and highlight functional deficits in current commercially-available prostheses.</p><p><strong>Results: </strong>Across all participants, 13 (54%) of the 24 trials resulted in a fall (defined as > 50% body-weight support) with all but one participant (83%) falling at least once and two participants (33%) falling every time. In contrast, in a previous study of seven young, unimpaired, non-prosthesis users using the same experimental apparatus, no falls occurred across 190 trials. For the transfemoral prosthesis users, early swing had the highest rate of falling at 64%, followed by mid-swing at 57%, and then late swing at 33%. The trend in falls was mirrored by the kinematic recovery metrics (peak trunk angle, peak trunk angular velocity, forward reach of the perturbed limb, and knee angle at ground contact). In early swing all four metrics were deficient compared to non-prosthesis user controls. In mid swing, all but trunk angular velocity were deficient. In late swing only forward reach was deficient.</p><p><strong>Conclusion: </strong>Based on the stumble recovery responses, four potential deficiencies were identified in the response of the knee prostheses: (1) insufficient resistance to stance knee flexion upon ground contact; (2) insufficient swing extension after a perturbation; (3) difficulty initiating swing flexion following a perturbation; and (4) excessive impedance against swing flexion in early swing preventing the potential utilization of the elevating strategy. Each of these issues can potentially be addressed by mechanical or mechatronic changes to prosthetic design to improve quality of recovery and reduce the likelihood a fall.</p>\",\"PeriodicalId\":16384,\"journal\":{\"name\":\"Journal of NeuroEngineering and Rehabilitation\",\"volume\":null,\"pages\":null},\"PeriodicalIF\":5.2000,\"publicationDate\":\"2024-07-13\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"https://www.ncbi.nlm.nih.gov/pmc/articles/PMC11245817/pdf/\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Journal of NeuroEngineering and Rehabilitation\",\"FirstCategoryId\":\"5\",\"ListUrlMain\":\"https://doi.org/10.1186/s12984-024-01402-0\",\"RegionNum\":2,\"RegionCategory\":\"医学\",\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"Q1\",\"JCRName\":\"ENGINEERING, BIOMEDICAL\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Journal of NeuroEngineering and Rehabilitation","FirstCategoryId":"5","ListUrlMain":"https://doi.org/10.1186/s12984-024-01402-0","RegionNum":2,"RegionCategory":"医学","ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"Q1","JCRName":"ENGINEERING, BIOMEDICAL","Score":null,"Total":0}
Factors leading to falls in transfemoral prosthesis users: a case series of prosthesis-side stumble recovery responses.
Background: Falls due to stumbling are prevalent for transfemoral prosthesis users and may lead to increased injury risk. This preliminary case series analyzes the transfemoral prosthesis user stumble recovery response to highlight key deficits in current commercially-available prostheses and proposes potential interventions to improve recovery outcomes.
Methods: Six transfemoral prosthesis users were perturbed on their prosthetic limb at least three times while walking on a treadmill using obstacle perturbations in early, mid and late swing. Kinematic data were collected to characterize the response, while fall rate and key kinematic recovery metrics were used to assess the quality of recovery and highlight functional deficits in current commercially-available prostheses.
Results: Across all participants, 13 (54%) of the 24 trials resulted in a fall (defined as > 50% body-weight support) with all but one participant (83%) falling at least once and two participants (33%) falling every time. In contrast, in a previous study of seven young, unimpaired, non-prosthesis users using the same experimental apparatus, no falls occurred across 190 trials. For the transfemoral prosthesis users, early swing had the highest rate of falling at 64%, followed by mid-swing at 57%, and then late swing at 33%. The trend in falls was mirrored by the kinematic recovery metrics (peak trunk angle, peak trunk angular velocity, forward reach of the perturbed limb, and knee angle at ground contact). In early swing all four metrics were deficient compared to non-prosthesis user controls. In mid swing, all but trunk angular velocity were deficient. In late swing only forward reach was deficient.
Conclusion: Based on the stumble recovery responses, four potential deficiencies were identified in the response of the knee prostheses: (1) insufficient resistance to stance knee flexion upon ground contact; (2) insufficient swing extension after a perturbation; (3) difficulty initiating swing flexion following a perturbation; and (4) excessive impedance against swing flexion in early swing preventing the potential utilization of the elevating strategy. Each of these issues can potentially be addressed by mechanical or mechatronic changes to prosthetic design to improve quality of recovery and reduce the likelihood a fall.
期刊介绍:
Journal of NeuroEngineering and Rehabilitation considers manuscripts on all aspects of research that result from cross-fertilization of the fields of neuroscience, biomedical engineering, and physical medicine & rehabilitation.