研究详述了运营商在瓦卡穆埃尔塔地区完井情况的演变

C. Carpenter
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引用次数: 0

摘要

本文由 JPT 技术编辑 Chris Carpenter 撰写,包含 SPE 212574 号论文 "从勘探到开发:该论文未经同行评审。 内乌肯盆地的运营商开发 Vaca Muerta 的结果各不相同。就完整论文中介绍的运营商而言,近 10 年前的垂直勘探井已经让位于目前的开发阶段,即针对不同着陆点的多水平井井场。作者讨论了作业者如何通过提高产量和缩短出井周期来提高效率和成本效益,同时通过减少作业对环境的影响来促进项目的长期可持续性。 作者重点介绍了多年来取得最大进展的作业者 A 油田。论文全文详细介绍了开发的勘探和评价阶段。试验阶段。该阶段的主要目标是验证之前确定的两个着陆区(即 B 区和 D 区)的生产力。完井。活动计划共钻了 12 口水平井,其中只有 10 口完井(两口井因钻井和套管完整性问题而损失)。油井横向长度在 1000 米至 1500 米之间。最终的油井结构由三串组成:13⅜英吋表层套管、9⅝英吋中间套管和 5½ 英吋生产套管。应用的完井技术是先堵后采(PnP),平均井段长度为 100 米。在 B 区进行了初步敏感性试验,设计了两种不同的处理规模(基础和替代),以评估对成本和生产性能的影响。结果显示,采用替代处理方法的油井产量较低。运行问题。操作问题包括套管限制(仅在 D 区的一口井在塞钻作业中发现过一次)和油井干扰(一口油井在回流期间,邻近新油井的产量发生了变化)。这是由于新井与原有油井之间的钻井条件导致间距缩小所致。该阶段显示,B 区的油井产量超出预期,而 D 区的油井产量不足。开发阶段 I:决定将该阶段的所有油井都安排在干气窗口试验区的东侧。做出这一决定的主要原因是,根据评价井的观测结果,预计该区域的二氧化碳产量较低。完井。最初的开发阶段考虑了 20 口水平井,主要针对 B 区。最终完成了 19 口井。最终的油井结构由三串组成:10¾ 英寸的表层套管、7⅝ 英寸的中间套管和最后 4½ 英寸的生产套管。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Study Details Evolution of Operator’s Completions in Vaca Muerta
This article, written by JPT Technology Editor Chris Carpenter, contains highlights of paper SPE 212574, “From Exploration to Development: The Completion Evolution in Vaca Muerta,” by Juan C. Bonapace, SPE, Luis A. Riolfo, and Rodrigo Zrain, Total, et al. The paper has not been peer reviewed. Operators in the Neuquén Basin have developed Vaca Muerta with different results. In the case of the operator whose work is featured in the complete paper, vertical exploratory wells almost 10 years ago have given way to a current development phase with multihorizontal well pads targeting different landings. The authors discuss how the operator has become more efficient and cost-effective by increasing production and reducing well-delivery-cycle time, while fostering the long-term sustainability of the project by reducing the environmental impact of operations. The authors focus on the operator’s Field A, where the most progress has been made over the years. The exploratory and appraisal phases of the development are detailed in the complete paper. Pilot Phase. The primary goal for this phase was to validate the productivity of two previously identified landing zones, namely Zones B and D. The wells were located near the vertical wells. Completion. The campaign program accounted for 12 drilled horizontal wells, only 10 of which were completed (two wells were lost because of drilling and casing-integrity issues). Well lateral length ranged between 1000 and 1500 m. The final well architecture was composed of three strings: a 13⅜-in. surface casing, a 9⅝-in. intermediate casing, and a 5½-in. production casing. The completion technique applied was plug-and-perf (PnP) and considered an average stage length of 100 m. Two base designs were defined for each landing zone according to the results obtained in the vertical exploratory wells. An initial sensitivity trial was completed in Zone B, with two different treatment sizes, base and alternative, designed to evaluate the effect on cost and production performance. The results showed a lower production for the wells with the alternative treatment. Operational Issues. Operational problems included casing restriction, detected only once in a well in Zone D during plug drillout operations; and well interference, in that one well presented a change in production during the flowback period on a new neighboring well. This was the result of reduced spacing because of drilling conditions between the new well and the pre-existing one. This phase showed wells in Zone B performing beyond expected production, while those in Zone D underperformed. Development Phase I. It was decided to locate all wells of this phase on the east side of the pilot in the dry-gas window. The main driver for this decision was expected lower CO2 production in this region, based on observations from appraisal wells. Completion. Initial development considered 20 horizontal wells, mainly targeting Zone B. Two additional target zones were added for testing, Zones A and C. In pursuing cost optimization for this development phase, a change to a slimmer architecture was made. Finally, 19 wells were completed. The final well architecture was composed of three strings: a 10¾-in. surface casing, a 7⅝-in. intermediate casing, and a final 4½-in. production casing.
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