叶尖摩擦是导致燃气轮机压缩机叶片故障的罕见冶金根源

A. Neidel, T. Gädicke, J. Rockel
{"title":"叶尖摩擦是导致燃气轮机压缩机叶片故障的罕见冶金根源","authors":"A. Neidel, T. Gädicke, J. Rockel","doi":"10.1515/pm-2023-0069","DOIUrl":null,"url":null,"abstract":"Abstract A heavy-duty gas turbine engine at the heart of a seawater desalination plant on the Arabian Peninsula exhibited multiple impact damages on their compressor airfoils that were detected during an inspection. Many blades showed heavily damaged airfoils and some even lost fractured-off parts. One moving blade in row 8 lost 50 % of its airfoil. Most compressor blade tips from stages 4 to 15 were damaged and bent. It was reported from the site that turning gear operation had been omitted once after engine shut-down in the recent past, i. e., the still hot rotor had not been turned until cool-down, resulting in rotor bend. This is believed to have caused the tip rubbing and airfoil break-off during the next engine start.","PeriodicalId":20360,"journal":{"name":"Practical Metallography","volume":null,"pages":null},"PeriodicalIF":0.0000,"publicationDate":"2023-11-24","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Tip Rubbing as a Rare Metallurgical Root Cause of Gas Turbine Compressor Blade Failure\",\"authors\":\"A. Neidel, T. Gädicke, J. Rockel\",\"doi\":\"10.1515/pm-2023-0069\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"Abstract A heavy-duty gas turbine engine at the heart of a seawater desalination plant on the Arabian Peninsula exhibited multiple impact damages on their compressor airfoils that were detected during an inspection. Many blades showed heavily damaged airfoils and some even lost fractured-off parts. One moving blade in row 8 lost 50 % of its airfoil. Most compressor blade tips from stages 4 to 15 were damaged and bent. It was reported from the site that turning gear operation had been omitted once after engine shut-down in the recent past, i. e., the still hot rotor had not been turned until cool-down, resulting in rotor bend. This is believed to have caused the tip rubbing and airfoil break-off during the next engine start.\",\"PeriodicalId\":20360,\"journal\":{\"name\":\"Practical Metallography\",\"volume\":null,\"pages\":null},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2023-11-24\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Practical Metallography\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.1515/pm-2023-0069\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Practical Metallography","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.1515/pm-2023-0069","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

摘要

摘要 位于阿拉伯半岛海水淡化厂中心的一台重型燃气涡轮发动机在检查过程中发现其压气机机翼有多处撞击损坏。许多叶片严重受损,有些甚至失去了断裂的部分。第 8 行的一个活动叶片的翼面损失了 50%。第 4 至第 15 级的大多数压缩机叶片尖端都有损坏和弯曲。据现场报告,不久前曾有一次在发动机关闭后省略了转动齿轮的操作,即在冷却之前没有转动仍处于高温状态的转子,导致转子弯曲。这被认为是在下一次启动发动机时造成尖端摩擦和机翼断裂的原因。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Tip Rubbing as a Rare Metallurgical Root Cause of Gas Turbine Compressor Blade Failure
Abstract A heavy-duty gas turbine engine at the heart of a seawater desalination plant on the Arabian Peninsula exhibited multiple impact damages on their compressor airfoils that were detected during an inspection. Many blades showed heavily damaged airfoils and some even lost fractured-off parts. One moving blade in row 8 lost 50 % of its airfoil. Most compressor blade tips from stages 4 to 15 were damaged and bent. It was reported from the site that turning gear operation had been omitted once after engine shut-down in the recent past, i. e., the still hot rotor had not been turned until cool-down, resulting in rotor bend. This is believed to have caused the tip rubbing and airfoil break-off during the next engine start.
求助全文
通过发布文献求助,成功后即可免费获取论文全文。 去求助
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术官方微信