小型涡喷发动机离心压气机叶片疲劳断裂事件分析

Songlin Qian, Wei Guo, Min Chen, Kunlin Lu, Lei Zhang, Yongxin Wu, Fei Wang
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引用次数: 0

摘要

在本研究中,对一台小型涡轮喷气发动机进行了性能验证试验,在试验过程中,离心压气机叶片根部发生了故障,叶片由铝合金制成。进行了详细的拆卸和检查,以查明故障的原因。研究发现,一个叶片根部的失效会导致其他叶片的卡死。然后,被卡住的叶片经历严重的摩擦和接触进气管道。材料性能的实验测量和制造过程的回顾性检查表明,材料的屈服强度低于设计值,叶片根部的圆角半径小于规格。本次压气机叶片疲劳失效的根本原因是加工质量和材料性能不合格,导致裂纹萌生和疲劳扩展直至失效。找出根本原因的经验将为其他小型涡轮喷气发动机提供工程指导。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Analysis of fatigue fracture incident of centrifugal compressor blades in a small turbojet engine
In this study, performance verification tests were conducted on a small turbojet engine, during which a failure occurred at the root of the centrifugal compressor blades, which are made of aluminum alloy. A detailed disassembly and inspection was carried out to reveal the reason of the failure. It was found that the failure of one blade at the root led to jamming of other blades. Then the jammed blades experience sever rubbing and contact with the intake duct. Experimental measurements of material properties and a retrospective examination of the manufacturing process revealed that the yield strength of the material was lower than the design value, and the fillet radius at the blade root was smaller than specifications. The root cause of the fatigue failure of the compressor blades in this incident was attributed to substandard machining quality and material properties, which leads to crack initiation and fatigue propagation until failure occurred. The experience of identifying the root cause would provide engineering guidance for other small turbojet engines.
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