将传统的机动钻井轨迹控制转变为自主旋转导向系统

Chinh Phan Van, Abdulqawi Al Fakih, Luis Felipe Gonzales, Anwar Faizd Osman
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引用次数: 0

摘要

在定向井钻井中,最具挑战性的段是曲线段。该曲线段以前使用传统的滑动/旋转导向电机进行钻井作业,但存在井眼清洁效率差和钻井时间延长的问题。旋转导向系统(RSS)是在一个交钥匙工程中引入的,它消除了滑动和旋转的限制,从而降低了每英尺的成本。最初,RSS的井下自动化仅限于控制垂直井和斜井。后来,闭环控制发展到保持倾角和方位角,但曲线部分仍然是非自动化的。司钻通过调整转向参数,继续手动钻进曲线段。最近,RSS中集成了一种新的自主井下控制系统(ADCS),可以实现曲线段的自主钻井,进一步减少人为不一致,提高井眼质量、钻井效率、井经济性,并减少碳足迹。对多口井进行了分析。研究了不同的BHA配置和不同的稳定器,以提高狗腿能力。收集了钻头记录并分析了其导向性和稳定性。重新设计了轨迹,以确保在规划阶段考虑到最小的狗腿严重性。这确保了在RSS的技术限制内,避免了由于无法保持轨迹而意外出井。具体的现场策略是通过智能规划、智能执行、地面自动化和井下自动化的数字化旅程来制定的。RSS与新开发的ADCS结合在一起,使司钻成为监控数字钻井系统的监督角色。RSS是在一个交钥匙工程中引入的,通过提高ROP,一次钻到鞋,有效地清洗井眼以避免卡钻事故,并为下套管和尾管提供更平滑的井眼,从而降低每英尺的成本。集成到RSS中的新型ADCS解决了自动化难题,并已在同一项目的许多井中成功进行了测试。它将人工决策转移到井下控制,在某些情况下,进一步提高了ROP高达100%,每口井最多可节省三天的时间。本文将详细介绍从泥浆马达到旋转导向系统(RSS)的弯曲段和水平段底部钻具组合的变化,以及井下自动化的重大进展,并展望全球类似领域自动钻井的未来。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Transforming the Trajectory Control from Conventional Motor Drilling to Autonomous Rotary Steerable Systems
The most challenging section in drilling directional wells is the curve section. This curve section used to be drilled by a conventional steerable motor with a slide/rotate decision with the greater challenges of poor hole cleaning efficiency and increased drilling time. The Rotary Steerable System (RSS) was introduced in a turnkey project by eliminating slide and rotate limitations to reduce the cost per foot. Initially, the downhole automation of the RSS was limited to holding verticals and inclinations. Later, the closed-loop control progressed to hold inclination and azimuth, but the curve section remained unautomated. The driller continued to drill the curve section manually by adjusting the steering parameters. A new Autonomous Downhole Control System (ADCS) recently integrated into the RSS enables autonomous drilling of the curve section, further reducing human inconsistencies and improving borehole quality, drilling efficiency, well economic, and reducing carbon footprint. Multiple offset wells were analyzed. Different BHA configurations were studied with various stabilizations to increase the dogleg capability. Bit records were gathered and analyzed for steerability and stability. The trajectory design was revisited to ensure minimum dogleg severity was considered at the planning stage. This ensured staying within the RSS's technical limits and avoiding unplanned pulling out of the hole due to failure to maintain the trajectory. The specific field strategy was prepared with the digital journey of intelligent planning, intelligent execution, surface automation, and downhole automation. The RSS was incorporated with the newly developed ADCS, placing the driller into the supervisory role to monitor the digital drilling system. The RSS was introduced in a turnkey project to reduce the cost per foot by improving the ROP, drilling shoe-to-shoe in one run, having efficient hole cleaning to avoid stuck pipe incidents, and having a smoother borehole for running casing and liner. The new ADCS incorporated into the RSS completed the automation puzzle and has been tested successfully in many wells on the same project. It transfers human decision-making to the downhole control, further increasing ROP in some cases by up to 100% and up to three days saved on each well drilled. This paper will illustrate the detailed BHA change in curved and horizontal sections from mud motor to the RSS with the significant progression of downhole automation and a future view for autonomous drilling in similar fields worldwide.
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