工程设计如何实现最长中间段的钻井

Amir Galaby, M. Cárdenas, H. Cengiz, B. R. Kosberg, Martin Sanderson, Ara Krikor
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引用次数: 1

摘要

由于对天然气的需求不断增加,以满足电力生产的需要,因此通常需要更多的替代天然气来源来应对夏季增加的需求。在伊拉克南部,这种情况是寻找经济上可行和有效的解决方案以寻找额外天然气资源的主要动力。因此,伊拉克政府接受挑战,钻探更深的含气地层,尽管在这些领域的经验有限。在2015年和2016年对这些气田进行的最新评估中,主要挑战之一是在钻过不同的互层和磨蚀地层时,钻头和底部钻具组合(BHA)发生故障。改变钻头类型、BHA集中、驱动系统和钻井参数并没有带来显著的效益。对于17.1 / 2”段,需要多达6次独立的下入才能成功钻完整个段。由于严重的冲击和振动,高轴向力和高扭矩导致井下泥浆马达和钻头失效,导致打捞作业和严重的非生产时间,因此成功的限制。此外,还存在钻井参数不稳定、机械钻速极低、井筒质量差等问题,这些问题会导致过度扩眼和反扩眼、卡钻事件以及难以保持井的垂直度。为了避免和减少这些挑战的影响,一个综合工程团队对BHA、钻头和所钻地层之间的相互作用进行了各种有限元分析。对邻井的保井条件、钻井液策略和钻井参数进行了重新分析。对钻头的选择进行了修改,确定了在切削齿和钻头剖面上引入适合用途的技术的机会。最终的挑战是一次钻完整个1800米的井段,避免任何与BHA相关的故障。在第四口井中,结果超出了预期,没有观察到BHA相关故障,钻头能够钻满1800米。连接实践也得到了优化。这使得基于井径测井的井眼质量得到了改善。改善的井眼条件使得套管下入和连续固井作业顺利进行。本文将讨论在伊拉克为数不多的天然气田之一实现这一重要里程碑所遵循的工程方法。详细介绍了BHA分析、钻头选择、钻井参数优化和钻井液策略实施等技术。本文的目的是与油气行业分享一种高效钻井的方法,以及如何通过技术引进和工程设计来解决钻井挑战。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
How Engineering Design Enabled Drilling the Longest Intermediate Section
As the demand for natural gas continuously increases to meet electricity production needs, more alternative natural gas sources are usually required to cope with the increased demand in the summer months. In South Iraq, this situation is the main driver for exploiting economically feasible and efficient solutions in finding additional natural gas resources. As a result, the Iraqi government embraces the challenge by drilling deeper formations which are gas bearing, with limited experience in such fields. In the most recent appraisal campaign for these gas fields, performed in 2015 and 2016, one of the main challenges were bits and bottom hole assembly (BHA) failures while drilling through different interbedded and abrasive formations. Changing the bits type, BHA centralization, drive system and drilling parameters did not result in significant benefits. For the 17 ½" section, up to six (6) independent runs were required to successfully drill the entire section. The success was limited due to severe shocks and vibrations, high axial forces and high torque that caused failures on downhole mud motors and bits, leading to fishing operation and severe non-productive time. Other problems like unstable drilling parameters, extremely low rate of penetration (ROP) and poor wellbore quality were observed, leading to excessive reaming and backreaming as well as stuck pipe events and difficulties to maintain well verticality. To avoid and minimize the impact of these challenges, a comprehensive engineering team performed various finite element analysis on the interaction between BHA, drilling bit and formations drilled. The conditions on which the wellbore was maintained in the offset wells with its drilling fluids strategy and drilling parameters were reanalyzed. The bits selections were revised, identifying areas of opportunity to introduce fit for purpose technologies on cutters and bits profile. The ultimate challenge was to drill the full 1800 m of the section in one run avoiding any BHA related failure. The results exceeded expectations in the fourth well, where no BHA related failures were observed, and the drilling bit was able to drill the full 1800 m. Connection practices were also optimized. This enabled an improvement in the wellbore quality based on caliper logs. Improved wellbore conditions allowed a smooth casing run and consecutive cement job. This paper will discuss the engineering methodology followed to achieve this important milestone in one of the few gas fields in Iraq. It will go through the details of the technologies implemented on BHA analysis, bit selection, drilling parameters optimization and drilling fluids strategy implemented. The objective of this paper is to share with the oil and gas industry a methodical approach for efficient drilling, and how to address drilling challenges with technology introduction and engineering design.
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