在0.65 /spl mu/m三层金属装置的制造环境中,合作提供快速提高产量的解决方案

G. Kong, J. W. Peterson, M. Cherniawski
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引用次数: 0

摘要

一个与速度有关的问题降低了0.65 /spl亩/米的三层金属装置的产量。减少信道长度是提高器件速度的最简单和最经济有效的方法。然而,过于激进的缩小通道长度也可能导致设备泄漏。为了确定具有足够速度性能且无泄漏的最佳通道长度,进行了一系列实验,建立了通道长度与器件阈值电压(Vt)的函数模型。通过调节通道植入物的剂量来改变Vt。通过调整曝光时间和轻掺杂漏极(LDD)植入物剂量来改变通道长度,而不是使用不同尺寸的掩模。这种方法大大降低了实验成本,缩短了学习周期。通过方差分析(ANOVA)在产率和p沟道晶体管长度之间建立了很强的相关性。定义了工作通道长度范围,其中通道长度越大,速度性能越差,通道长度越小,器件泄漏。增加曝光时间的临时工艺立即实施,以确保模具出货数量和交货进度。同时,确定了最佳掩模尺寸,并重新生成了这个掩模,这样当使用这个掩模时,原始照片的曝光将重新集中在过程中。然后取消了中间工序,以简化可制造性。优化后的工艺显著提高了收率。在设备工程、工艺工程和制造团队之间建立了强有力的合作伙伴关系,以在不影响可制造性和客户交付的情况下及时实现产量提高。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Partnership for a rapid yield enhancement solution in a manufacturing environment on a 0.65 /spl mu/m triple level metal device
A speed related problem degraded the yield of a 0.65 /spl mu/m triple level metal device. Reducing the channel length was the most simple and cost effective approach to improve device speed. However, an overly aggressive downsized channel length could also cause device leakage. To determine the optimal channel length with adequate speed performance and without leakage, a series of experiments were run to establish a yield model as a function of channel length and device threshold voltage (Vt). The Vt was varied by adjusting the channel implant dose. Instead of using masks with different sizings, the channel length was varied by adjusting photo exposure time and lightly doped drain (LDD) implant dose. This approach greatly reduced the cost of experiments and shortened the learning cycle. A strong correlation was established by Analysis of Variances (ANOVA) between yield and p-channel transistor length. The range of operational channel length was defined, where higher channel length caused poor speed performance and lower channel length caused device leakage. An interim process with increased photo exposure time was implemented immediately to ensure die shipment quantity and delivery schedule. In parallel, the optimal mask sizing was determined and this mask regenerated such that the original photo exposure when used with this mask would re-center the process. The interim process was then eliminated to streamline manufacturability. The optimized process resulted in significant yield improvement. Strong partnerships were established among device engineering, process engineering, and manufacturing groups to achieve yield enhancement in a timely manner without compromising manufacturability and customer deliveries.
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