核电站蒸汽发生器热性能退化问题研究

Qing-Sen Zhao, Ying-Jie Chu, W. Luo, Wei-rang Wu, Yuying Kong
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引用次数: 0

摘要

与任何热交换器一样,核蒸汽发生器的功能会受到操作变化的影响,这些变化会增加一次流体和二次流体之间的传热阻力,从而降低效率并导致热性能下降。ERRI和DEI参考文档已经讨论了这种类型的性能下降、潜在原因、行业经验和工厂操作后果。运行6 ~ 10年后,大部分电厂蒸汽压力下降。宁德核电站投入商业运行后,蒸汽发生器蒸汽压力下降。第一次燃料循环降低了1 bar,第二次和第三次燃料循环降低了0.5 bar。而法国的同类型核电站没有类似的情况。美国部队的情况也不同。本文认为,造成蒸汽压力损失的主要原因是二回路管道和支撑板处淤积的污泥或污垢。涡流成像和视频检测结果表明,靠近管支承板1的冷侧管有污泥或沉淀物,热侧管的污泥量小于冷侧管。一般情况下,上管束未见沉积信号。SG管上的污泥总量较少,这可能与污染因素相矛盾。宁德核电站1号机组采用束式冲洗设备,污泥量是普通管板式冲洗的5倍。这种特殊的束式冲洗应用减少了SGs中的污泥,避免了传热管的腐蚀,确保了SGs的安全。遗憾的是,经过这次特殊冲洗后,SG的热性能没有迅速恢复。TSP1附近的污泥不是蒸汽压力损失的主要原因。目前,项目组正在研究聚丙烯酸(PAA)和化学清洗,以扩大清洗范围和清洗效果,进一步恢复蒸汽发生器的热工性能。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
The Research of Steam Generator Thermal Performance Degradation in Nuclear Power Plant
As with any heat exchanger, the function of a nuclear steam generator is compromised by operational changes that increase the resistance to heat transfer between the primary and secondary fluids, lowering the efficiency and leading to thermal performance degradation. This type of performance degradation, the underlying causes, industry experience, and plant operational consequences had been discussed by ERRI and DEI reference documentations. After 6–10 years operation the steam pressure degradation of most plants occurred. The steam pressure of steam generator (SG) in Ningde nuclear power plant (NPP) decreased after the unit was in commercial operation. It decreased by 1 bar in first fuel cycle, and it was down by 0.5 bar at the second and third cycle. And the same type of nuclear power plant in France had no similar status. It was also different with the situations of American units. In this paper it concludes that the main cause of steam pressure loss is the sludge or fouling which accumulated at tubes and supporting plates at the second loop. The eddy current imaging and video inspection results showed that the sludge or deposit were found at the cold side tubes nearby the tube supporting plate one, the sludge amount at hot side tubes was smaller than the cold tubes. In general, there were no deposit signals at the upper tube bundle. And the total amount of sludge on SG tubes was fewer, which was possibly contradiction with the fouling factor. The bundle flushes equipment have been applied at Ningde NPP unit 1, the sludge amount was five times larger than the normal tube sheet flush. This special bundle flush applications reduce the sludge in the SGs, avoid the corrosion of heat transfer tubes and ensure the SGs safety. It is a pity that the SG thermal performance was not recovered quickly after this special flush. The sludge nearby the TSP1 was not the main cause of steam pressure loss. At present, the project team is studying polyacrylic acid (PAA) and chemical cleaning to expand the scope of washing and cleaning effect, and further recover the thermal performance of steam generator.
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