焊接锅炉管在弯曲操作过程中的失效

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引用次数: 0

摘要

在试图操纵或弯曲约22英尺长的锅炉管时,突然发生故障,似乎是管中的对接焊缝。在外部,焊接加固已经地面平齐,整个管表面涂漆。在内部,加热带的外观和宽度表明焊接是由氧气工艺制成的。在它的大部分长度上缺乏根融合是明显的。断口表面呈结晶状,表明脆性行为,表明焊缝根部未完全融合。显微检查表明,该矿床具有大晶粒尺寸,低碳含量沿晶界以碳化物的形式分布,这一特征可以解释脆性行为。随后的检查表明,该管是为锅炉重新管道订购的几个批次之一,其中一端焊接有2英尺长,以弥补长度。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure of a Welded Boiler Tube During a Bending Operation
On attempting to manipulate or bend a boiler tube some 22 ft. long, sudden failure occurred at what appeared to be a butt weld in the tube. Externally, the weld reinforcement had been ground flush and the entire tube surface painted. Internally, the appearance and width of the heated band suggested that the weld had been made by the oxy-gas process. A lack of root fusion over most of its length was evident. Examination of the fracture faces, which were of crystalline appearance indicative of brittle behavior, indicated incomplete fusion of the weld root. Microscopic examination showed the deposit to possess a large grain size with a low carbon content disposed as carbides along the grain boundaries, a feature which would provide an explanation of the brittle behavior. Subsequent inspection showed that this tube was one of several of the batch ordered for retubing of a boiler and which had a 2 ft. length welded to one end to make up the length.
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