井下安全阀流管在e -管线上磨铣成功后,恢复了生产和油井通道,避免了大规模的钻机修井

Juan Jose Nobile Blanco, S. Prabhakaran, Shiwanshu Shiwan, Chirag Rathod, David Ting
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摘要

在流入测试失败后,一口海上生产井停止了作业。设计了补救工作计划,但执行过程中导致地下安全阀(SSSV)内流管顶部严重损坏,导致弯曲,无法生产。利用机器人工具进行电缆输送机械修井作业,磨铣堵塞物,恢复全井眼通道。井下硬件磨铣是一种常见的技术;然而,为了成功,必须遵循一个彻底的过程。需要考虑的因素包括:井的结构(完井示意图和限制条件);流管材质为9CR-1MO马氏体钢;破坏周边地区的风险;铣削时旋转整个总成的风险;同时也存在被井下钻具组合(BHA)卡住的风险。铣磨干预方案的起草考虑了不同的情况,包括突发事件。由于作业的紧迫性和铣削后SSSV的高精度要求,E-line传输的机器人铣削干预是首选。机器人工具串首先用于下入。随后进行的诊断下入有助于团队了解井下情况,调整作业计划,并测试井下工具的性能。最后,磨铣作业在采集系统上显示了一个明确的签名,为相关各方提供了关于结果的确定性。进行了一次摄像机下入,以验证磨铣后作业区域的条件。根据程序,该作业总共运行了四次。此外,铣削时间本身仅为17分钟。在SSSV功能齐全的情况下,客户可以在测试完井的完整性后立即恢复生产。本文描述了一种复杂但高效的作业,通过电缆输送的机器人铣削工具能够消除关键的井下障碍,恢复生产,同时保持井的所有安全特征,从而避免了复杂的修井作业。经过深入的准备工作,然后有条不紊地执行,这口井恢复了石油生产。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Production and Well Access Restored After a Successful Subsurface Safety Valve Flowtube Milling on E-line, Preventing Major Rig Workover
An offshore production well was out of operation after unsuccessful inflow tests. A remedial work plan was designed, but the execution resulted in severe damage to the top of the flowtube inside the Subsurface Safety Valve (SSSV), which was bent over and preventing production. Wireline conveyed mechanical intervention was performed with robotic tools to mill the obstruction and regain full bore access. Downhole hardware milling is a common technology; however, a thorough process must be followed in order to succeed. The following factors were among those to be considered: well configuration (completion schematic and restrictions); the material of the flowtube (9CR-1MO Martensitic Steel); the risk of damaging the surrounding area; the risk of rotating the whole assembly while milling; and the risk of getting stuck with the e-line Bottom Hole Assembly (BHA). The milling intervention program was drafted taking into consideration different scenarios including contingencies. E-line conveyed robotic milling intervention was the preferred option due to the urgency of the operation and high accuracy required to ensure the SSSV was left operational after milling. The robotic toolstring was first deployed for a drift run. Subsequent diagnostic runs were executed to help the team understand the downhole situation, adjust the operation plan and to test the performance of the tool downhole. Finally, the milling run was conducted showing a clear signature on the acquisition system, providing the parties involved with certainty regarding the outcome. A camera run was performed to verify the conditions of the operational area after milling. The job was executed in a total of four runs as per the program. Furthermore, the milling time itself was only 17 minutes. The complete removal of the damaged section of flowtube allowed the client to restore production immediately after testing the well integrity, with the SSSV fully functional. This paper describes the complex yet efficient operation where a robotic milling tool, conveyed by e-line, was able to remove a critical downhole obstruction and restore production while preserving all safety features of the well, thus preventing a complex workover operation. The in-depth preparation, followed by a methodical execution, allowed oil production to be resumed in this well.
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