核设施水密门水密性检验分析(超出设计条件的水密性)

Hideto Taoka, Nobuo Ishida, T. Toriyama
{"title":"核设施水密门水密性检验分析(超出设计条件的水密性)","authors":"Hideto Taoka, Nobuo Ishida, T. Toriyama","doi":"10.1299/transjsme.20-00045","DOIUrl":null,"url":null,"abstract":"A test on the water tightness performance of watertight doors was conducted to obtain knowledge on the fragility beyond design conditions. The performance test was conducted on three types of standard single-swinging watertight doors used for nuclear facilities. Assuming tsunami conditions during an earthquake, the water pressure and the shear strain caused by horizontal force were applied on the watertight door during the test. A shear strain of up to 4000 μ and a water pressure of up to 0.3 MPa were loaded step by step. The water that leaked from the door was measured at each step. The test results showed that the water pressure was related to the leakage quantities, but no clear relationship was observed between the shear strain and leakage quantities. Subsequently, a confirmation test was conducted focusing on the sealed portion of the watertight doors. The condition of the packing and the leakage of the seal during water pressure loading was observed. Consequently, we found that a large quantity of leakage under water pressure was caused by protrusion of the packing, and we inferred that leakage would occur by the same mechanism in actual watertight doors. Using the test results, we considered a method for evaluating the water tightness limit of the door. An analysis on the performance test was conducted using the evaluation method. The result showed that the water pressure that formed a leakage path in the analysis was consistent with the water pressure that caused a large quantity of leakage in the test.","PeriodicalId":341040,"journal":{"name":"Transactions of the JSME (in Japanese)","volume":"123 5 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"1900-01-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Examination and analysis of the water tightness of watertight doors in nuclear facilities (Water tightness of the watertight doors beyond design conditions)\",\"authors\":\"Hideto Taoka, Nobuo Ishida, T. Toriyama\",\"doi\":\"10.1299/transjsme.20-00045\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"A test on the water tightness performance of watertight doors was conducted to obtain knowledge on the fragility beyond design conditions. The performance test was conducted on three types of standard single-swinging watertight doors used for nuclear facilities. Assuming tsunami conditions during an earthquake, the water pressure and the shear strain caused by horizontal force were applied on the watertight door during the test. A shear strain of up to 4000 μ and a water pressure of up to 0.3 MPa were loaded step by step. The water that leaked from the door was measured at each step. The test results showed that the water pressure was related to the leakage quantities, but no clear relationship was observed between the shear strain and leakage quantities. Subsequently, a confirmation test was conducted focusing on the sealed portion of the watertight doors. The condition of the packing and the leakage of the seal during water pressure loading was observed. Consequently, we found that a large quantity of leakage under water pressure was caused by protrusion of the packing, and we inferred that leakage would occur by the same mechanism in actual watertight doors. Using the test results, we considered a method for evaluating the water tightness limit of the door. An analysis on the performance test was conducted using the evaluation method. The result showed that the water pressure that formed a leakage path in the analysis was consistent with the water pressure that caused a large quantity of leakage in the test.\",\"PeriodicalId\":341040,\"journal\":{\"name\":\"Transactions of the JSME (in Japanese)\",\"volume\":\"123 5 1\",\"pages\":\"0\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"1900-01-01\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Transactions of the JSME (in Japanese)\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.1299/transjsme.20-00045\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Transactions of the JSME (in Japanese)","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.1299/transjsme.20-00045","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

摘要

通过对水密门的水密性能试验,了解了水密门在设计条件下的易损性。对三种核设施标准单摆水密门进行了性能试验。在假定地震时发生海啸的条件下,对水密门施加水压和水平力引起的剪切应变。在最高可达4000 μ的剪切应变和最高可达0.3 MPa的水压下逐级加载。门上漏出的水每走一步都要量一量。试验结果表明,水压与泄漏量有关,但剪切应变与泄漏量无明显关系。随后,对水密门的密封部分进行了确认试验。观察了水压加载过程中填料和密封的泄漏情况。因此,我们发现在水压下大量的泄漏是由于填料的突出引起的,我们推断在实际的水密门中也会以同样的机制发生泄漏。根据试验结果,提出了一种门的水密极限评价方法。采用评价方法对性能试验进行了分析。结果表明,分析中形成泄漏路径的水压与试验中造成大量泄漏的水压一致。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Examination and analysis of the water tightness of watertight doors in nuclear facilities (Water tightness of the watertight doors beyond design conditions)
A test on the water tightness performance of watertight doors was conducted to obtain knowledge on the fragility beyond design conditions. The performance test was conducted on three types of standard single-swinging watertight doors used for nuclear facilities. Assuming tsunami conditions during an earthquake, the water pressure and the shear strain caused by horizontal force were applied on the watertight door during the test. A shear strain of up to 4000 μ and a water pressure of up to 0.3 MPa were loaded step by step. The water that leaked from the door was measured at each step. The test results showed that the water pressure was related to the leakage quantities, but no clear relationship was observed between the shear strain and leakage quantities. Subsequently, a confirmation test was conducted focusing on the sealed portion of the watertight doors. The condition of the packing and the leakage of the seal during water pressure loading was observed. Consequently, we found that a large quantity of leakage under water pressure was caused by protrusion of the packing, and we inferred that leakage would occur by the same mechanism in actual watertight doors. Using the test results, we considered a method for evaluating the water tightness limit of the door. An analysis on the performance test was conducted using the evaluation method. The result showed that the water pressure that formed a leakage path in the analysis was consistent with the water pressure that caused a large quantity of leakage in the test.
求助全文
通过发布文献求助,成功后即可免费获取论文全文。 去求助
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术官方微信