在不增加投资的情况下,16mb dram栅极导体刻蚀的生产率提高30%

U. Rogatty, F.G. Boebel
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引用次数: 2

摘要

对于今天的大批量16mb dram制造工艺优化和提高工具利用率是获得最大生产力的关键。作者详细展示了他们是如何实现栅极导体蚀刻工艺生产率提高30%的。特别强调了用于分析过程、过程流和工具集的方法。详细说明了修改后的工艺步骤。对聚类4室AMAT P5000 MarkII蚀刻工艺(Capoxide/Wsix/Strip/Poly)的仔细分析表明,最大吞吐量由最慢的单原始工艺时间(RTP)决定。通过拆解该过程,我们能够根据每个单个蚀刻步骤的RPT重新安排蚀刻室的数量,因此优化了可用蚀刻室的利用率。进一步的改进是通过修改WSix蚀刻工艺,引入HARDMASK,并在独立的FUSION和FSI工具上移动电阻条,这些工具也用于另一个工艺。本文表明,由于聚类过程。四腔蚀刻工具的总运行时间增加了。与之前的情况相比,所有这些综合改进提高了生产率,提高了约30%的晶圆吞吐量。资本投资不到30万美元,无需购买进一步的蚀刻工具。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
30% productivity increase of 16 Mb-DRAM gate-conductor etching without additional investment
For today high volume 16 Mb-DRAM manufacturing process optimization and increase of tool utilization is a key importance to gain maximum productivity. The authors show in detail how they achieved a 30% productivity increase for the gate conductor etch process. Special emphasis was put on the methodology used for analysis of process, process-flow and tool set. The modified process steps are explained in detail. The careful analysis of a clustered 4 chamber AMAT P5000 MarkII etch process (Capoxide/Wsix/Strip/Poly) showed that the maximum throughput was gated by the slowest single raw process time (RTP). By declustering the process, we were able to rearrange the number of etch chambers according to the RPT of each single etch step and therefore the utilisation of the available etch chambers was optimized. A further improvement was achieved by modifying the WSix etch process, introducing a HARDMASK and moving the resist-strip on stand-alone FUSION and FSI tools, which were used in another process as well. This paper shows that due to the declustered process. The combined uptime of the 4-chamber etch tools was increased. All combined improvements gave a productivity increase and improved wafer throughput of about 30% compared to the situation before. The capital investment was less than 300K$ and no further etch tools had to be purchased.
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