用孔眼和吸气法改造底围裙/鼻条对环纱纱线质量的影响

Bantamlak Birlie, Sampath Rangaraj
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引用次数: 1

摘要

目前环锭纺纱存在纤维集成度差的缺点,纤维从纱线表面突出,造成毛羽和不规则。本研究的目的是在传统瑞特G35环锭机上,通过改造带孔洞的底围裙/鼻条,并采用吸风的方法,纺纱29.52特级(20ne)和14.76特级(40ne),以提高纱线质量。为制备改性纱,采用17种胶圈孔径、吸纱压力和宽度孔距的组合。方差分析结果表明,随着吸力压力的增加,毛羽、韧性和厚度(+50%/km)都得到了显著改善。在此基础上,将吸力压力、胶圈孔直径和孔距分别优化为23.9 mbar、1.58 mm和10 mm, 40 mbar和25 mbar, 20 Ne分别为1.75 mm和11.6 mm。40 Ne改性纱线的毛羽、强力、细处和粗处分别比常规纱线提高了16.25%、12.7%、17.42%和14.62%。而20 Ne改性纱的毛羽、强力和粗度分别提高了8.87%、7.42%和18.2%。因此,改进后的G35缩纱方法可以生产出质量更好的纱线,可以作为常规纺纱的替代方法。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Investigation of Yarn Quality in Ring Yarn by Modifying Bottom Apron/Nose Bar with Perforations and Air-Suction
Currently, ring spinning has limitations of poor integration of fibers that protrude from yarn surface, which causes hairiness and irregularity. The aim of this research is to improve yarn quality by modification of bottom apron/nose bar with perforation and applying air-suction in a conventional Reiter G35 ring frame and spinning 29.52 Tex (20 Ne) and 14.76 Tex (40 Ne). To produce modified yarn 17 combinations of apron hole diameter, suction pressure, and widthwise hole distance was used. The ANOVA result shows that as suction pressure increases hairiness, tenacity, and thick place (+50%/km) were improved significantly for both counts. Based on the result suction pressure, apron hole diameter, and hole distance were optimized to 23.9 mbar, 1.58 mm and 10 mm respectively for 40 Ne and 25 mbar, 1.75 mm, and 11.6 mm respectively for 20 Ne. As compared with conventional hairiness, tenacity, thin place, and thick place of 40 Ne modified yarn were improved by 16.25%, 12.7%, 17.42%, and 14.62% respectively. Whereas hairiness, tenacity, and thick place of 20 Ne modified yarn were improved by 8.87%, 7.42%, and 18.2% respectively. Thus, the modified G35 method of yarn condensing has capability to be used as an alternative method of conventional spinning as it is capable of producing better quality yarn.
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