铬合金800管道系统故障

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引用次数: 0

摘要

某蒸汽重整装置出口管道系统因四个焊缝处大面积开裂而失效。焊接系统由铬合金800 (Fe-32Ni-21Cr-0.05C)管和管件组成。系统的外表面用岩棉绝缘,不含防风雨材料。现场目视检查和磁测表明,大部分管道外部腐蚀严重。该体系焊缝热影响区出现大面积开裂。一个试样表明,腐蚀扩展到3.2 mm的深度,在覆盖头的边缘和焊缝的热影响区可以看到裂纹。金相检验表明,裂纹是沿晶开裂,相邻晶界受到了深的沿晶攻击。在高倍镜下检查发现大量碳化物析出,主要在晶界处,表明合金被敏化了,这是焊接过程中加热造成的。电子探针x射线显微分析显示,管的外表面没有通常在铬合金800上发现的保护性氧化铬垢。管内表面有一层薄薄的氧化铬保护层。结果表明,深度氧化大大降低了焊缝热影响区强度,并导致开裂。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure of an Incoloy 800 Piping System
The outlet-piping system of a steam-reformer unit failed by extensive cracking at four weld locations. The welded system consisted of Incoloy 800 (Fe-32Ni-21Cr-0.05C) pipe and fittings. The exterior surfaces of the system were insulated with rock wool that did not contain weatherproofing. On-site visual examination and magnetic testing indicated severe external corrosion of most of the piping. The system showed extensive cracking in weld HAZ. One specimen indicated that corrosion extended to a depth of 3.2 mm and cracks were seen at the edge of the cover bead and in the HAZ of the weld. Metallographic examination showed that cracking was intergranular and that adjacent grain boundaries had undergone deep intergranular attack. Examination at higher magnification revealed heavy carbide precipitation, primarily at grain boundaries, indicating that the alloy had been sensitized, which resulted from heating during welding. Electron probe x-ray microanalysis showed the outside surface of the tube did not have the protective chromium oxide scale normally found on Incoloy 800. The inside surface of the tube had a thin chromium oxide protective scale. This evidence supported the conclusions that the deep oxidation greatly decreased the strength of the weld HAZ and cracking followed.
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