Kii-channel高压直流线路与立花湾1号机组孤岛系统模式试验

Y. Shimura, S. Hara, N. Uehara
{"title":"Kii-channel高压直流线路与立花湾1号机组孤岛系统模式试验","authors":"Y. Shimura, S. Hara, N. Uehara","doi":"10.1109/PESW.2001.917218","DOIUrl":null,"url":null,"abstract":"On May 24, 2000, the islanded system mode test of Kii-channel HVDC Link (bipolar, 1400 MW) and Tachibana-bay unit 1 (cross-compound, coal-fired, 1050 MW) was performed during its commissioning tests. Both the HVDC system and the generator continued to operate stably during islanded system mode. About 20 minutes later, the system was connected to the AC system again by re-closing the circuit breaker that was hand-tripped, and the system was restored. This paper presents the results of the islanded system mode test. The performance of some functions implemented to be able to operate in the islanded system mode was verified. The torsional vibration observed on the turbine-shaft was in stability, the contribution to the damping of SSDC was verified. Frequency of the islanded system was maintained at 60.0 Hz for 20 minutes owing to the frequency controller.","PeriodicalId":253534,"journal":{"name":"2001 IEEE Power Engineering Society Winter Meeting. Conference Proceedings (Cat. No.01CH37194)","volume":"18 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2001-01-28","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"2","resultStr":"{\"title\":\"Islanded system mode test of Kii-channel HVDC link and Tachibana-bay unit 1\",\"authors\":\"Y. Shimura, S. Hara, N. Uehara\",\"doi\":\"10.1109/PESW.2001.917218\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"On May 24, 2000, the islanded system mode test of Kii-channel HVDC Link (bipolar, 1400 MW) and Tachibana-bay unit 1 (cross-compound, coal-fired, 1050 MW) was performed during its commissioning tests. Both the HVDC system and the generator continued to operate stably during islanded system mode. About 20 minutes later, the system was connected to the AC system again by re-closing the circuit breaker that was hand-tripped, and the system was restored. This paper presents the results of the islanded system mode test. The performance of some functions implemented to be able to operate in the islanded system mode was verified. The torsional vibration observed on the turbine-shaft was in stability, the contribution to the damping of SSDC was verified. Frequency of the islanded system was maintained at 60.0 Hz for 20 minutes owing to the frequency controller.\",\"PeriodicalId\":253534,\"journal\":{\"name\":\"2001 IEEE Power Engineering Society Winter Meeting. Conference Proceedings (Cat. No.01CH37194)\",\"volume\":\"18 1\",\"pages\":\"0\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2001-01-28\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"2\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"2001 IEEE Power Engineering Society Winter Meeting. Conference Proceedings (Cat. No.01CH37194)\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.1109/PESW.2001.917218\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"2001 IEEE Power Engineering Society Winter Meeting. Conference Proceedings (Cat. No.01CH37194)","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.1109/PESW.2001.917218","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 2

摘要

2000年5月24日,Kii-channel HVDC Link(双极,1400mw)和立花湾1号机组(交叉复合,燃煤,1050mw)在调试试验中进行了孤岛系统模式试验。在孤岛系统模式下,高压直流系统和发电机继续稳定运行。大约20分钟后,通过重新闭合手动跳闸的断路器,系统重新连接到交流系统,系统恢复正常。本文介绍了孤岛系统模态试验的结果。验证了在孤岛系统模式下能够运行的一些功能的性能。在涡轮轴上观察到的扭转振动是稳定的,验证了SSDC对阻尼的贡献。由于频率控制器,孤岛系统的频率维持在60.0赫兹20分钟。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Islanded system mode test of Kii-channel HVDC link and Tachibana-bay unit 1
On May 24, 2000, the islanded system mode test of Kii-channel HVDC Link (bipolar, 1400 MW) and Tachibana-bay unit 1 (cross-compound, coal-fired, 1050 MW) was performed during its commissioning tests. Both the HVDC system and the generator continued to operate stably during islanded system mode. About 20 minutes later, the system was connected to the AC system again by re-closing the circuit breaker that was hand-tripped, and the system was restored. This paper presents the results of the islanded system mode test. The performance of some functions implemented to be able to operate in the islanded system mode was verified. The torsional vibration observed on the turbine-shaft was in stability, the contribution to the damping of SSDC was verified. Frequency of the islanded system was maintained at 60.0 Hz for 20 minutes owing to the frequency controller.
求助全文
通过发布文献求助,成功后即可免费获取论文全文。 去求助
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:604180095
Book学术官方微信