相互连接的过程调查,以解决分层

Bobe Lee, S. Chou
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引用次数: 0

摘要

模料与模具、模桨和内导联界面的分层研究已经进行了相当长的一段时间。这是一种慢性缺陷,如果分层渗透到模具复合材料与模具表面和模具复合材料与内引线的界面,将导致电气连续性故障,例如,热应力后,内引线或模具表面的分层导致断线。为了解决分层问题,需要更好的材料,如引线框架、模具附件和模具复合材料。除此之外,流程优化也是实现无分层结果的必要条件。本文描述了改进BOM后的分层现象,如降低吸水性和提高黏附力的模具化合物。在鉴定阶段,热应力后未发生分层。但是,在批量生产运行中,通过抽样检查,内部引线会发生分层。四个“M”字,材料,方法和机器进行了彻底的检查,并与其合格建造和量产运行进行了比较。不能观察到任何差异或结论。但是,分层是存在的,虽然没有发现/差异观察。然而,可以得出一个结论,资格是小体积,而质量确认运行是大体积。在此假设的基础上,对小体积和大体积进行分层比较,检查差异。然后,根本原因是模具附着放气,造成污染的包装是观察。经热处理后,污染物转化为分层。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Inter-connecting process investigation to resolve delamination
Delamination on the interface between mold compound to die, die paddle and inner leads study has been on-going for quite some time. This is a chronicle defect which will result in electrical continuity failure if delamination penetrates into the interface of mold compound to die surface and mold compound to inner leads e.g., delamination on inner leads or die surface to cause wire broken after thermal stress. To resolve delamination, better materials are needed such as Lead frame, die attach and mold compound. Other than that, a process optimization is also a must to achieve delamination free result. The paper portrays the phenomenon of how delamination occurred after improving the BOM e.g., less water absorption and higher adhesion mold compound. During qualification stage, no delamination occurred after thermal stress. But, on mass volume production run, the delamination occurs on inner leads by sampling check. Four “M” Men, Material, Method and Machines are thoroughly checked and compared with its qualification built and mass production run. No difference or conclusion can be observed and made. But, the delamination was there though no finding/difference was observed. However, one conclusion can be made is qualification is small volume but mass confirmation run is large volume. Based on the assumption, Delamination comparison between small volume VS. large volume was conducted to check the difference. Then, the root cause as die attach outgassing to cause contamination on package is observed. The contamination is later turn into delamination after Thermal.
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