由锻造飞机轮毂半部分的材料缺陷引起的疲劳裂纹

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引用次数: 0

摘要

一架商用飞机的轮毂一半是由2014年的铝合金锻件加工而成,经过热处理至T6回火,由于在例行检查中发现油坝半径区域存在裂纹,因此被停止使用。着陆的总次数和滚转里程都没有报告,但是从制造日期到轮子停止使用的日期已经过去了大约300天。分析(目视、宏观、显微、电子探针)支持了车轮半失效的结论。由于车轮旋转方向的改变改变了施加应力的方向,疲劳裂纹起源于材料缺陷,并在多个平面上发展。建议包括重新编写检验规范,要求锻件声音良好。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Fatigue Cracking That Originated at a Material Defect in a Forged Aircraft Wheel Half
A commercial aircraft wheel half, machined from an aluminum alloy 2014 forging that had been heat treated to the T6 temper, was removed from service because a crack was discovered in the area of the grease-dam radius during a routine inspection. Neither the total number of landings nor the roll mileage was reported, but about 300 days had elapsed between the date of manufacture and the date the wheel was removed from service. The analysis (visual inspection, macrographs, micrographs, electron microprobe) supported the conclusions that the wheel half failed by fatigue. The fatigue crack originated at a material imperfection and progressed in more than one plane because changes in the direction of wheel rotation altered the direction of the applied stresses. Recommendations included rewriting the inspection specifications to require sound forgings.
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