利用郭加拉伯的气液速率窗评价K-01地热井加气钻井效果

R. Wardana
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引用次数: 0

摘要

地热钻井中常见的问题是漏失问题。利用漏失材料(LCM)是解决漏失问题的常用方法之一,但在生产区域使用LCM会对生产区域造成破坏。因此,欠平衡钻井是防止地热井产层漏失的一种有效方法。最常见的欠平衡钻井方法之一是充气钻井或泡沫钻井。为了解决K-01地热井采区的漏失问题,采用了充气钻井。尽管已经使用了充气钻井,但仍然存在漏失问题。本研究的目的是利用Guo Ghalambor的气液速率窗口对K-01井的加气钻井作业进行评价,并提出下一步钻井作业的推荐气液速率。结合K-01地热井充气钻井的地层特征、钻井参数、钻井日报表及流体注入特征,构建气液速率窗口。利用构建的气液速率窗口,对K-01地热井的钻井作业进行了评价。通过检查泥浆测井数据中的漏失循环事件,评估加气钻井作业中使用的气液速率参数。在对充气钻井进行评价后,对下一步的钻井作业提出了建议。根据评价,K-01井9.875”井段使用的气液组合速率位于所建GLRW的外侧,因此出现了漏失循环问题。本研究推荐的气液复合速率可用于确定气液复合速率,以防止漏失循环、井筒破坏和岩屑输送问题。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Evaluation of Aerated Drilling in K-01 Geothermal Well using Guo Ghalambor’s Gas-Liquid Rate Window
Common problem in geothermal drilling is loss circulation problem. One of the common methods to cure loss circulation problem is using Lost Circulation Materials (LCM), but in the production zone, using LCM can damage the production zone. Therefore, underbalanced drilling is method that can be used to prevent loss circulation problems in production zone in geothermal well. One of the most common underbalanced drilling methods is aerated drilling or foam drilling. Aerated drilling was used to overcome the loss of circulation problem in production zone in K-01 Geothermal Well. Even though, the aerated drilling was already used, but the loss circulation problem was still occurred. The purpose of this research is to evaluate aerated drilling operation in K-01 Well using Guo Ghalambor’s Gas-Liquid Rate Window and make recommended gas-liquid rate for the next drilling operation. Gas-Liquid Rate Window is constructed using characteristic of the formation, drilling parameters, daily drilling report and also fluid injection characteristics that was used for aerated drilling operation in K-01 geothermal well. Using the constructed Gas-Liquid Rate Window, an evaluation is carried out for the drilling operation in K-01 geothermal well.  The gas-liquid rate parameters used in aerated drilling operations is evaluated while checking the loss circulation event from the mud logging data. After the evaluation of the aerated drilling is carried out in then a suggestion is made for the next drilling operation. Based on the evaluation, the combination of gas-liquid rates that was used on the 9.875"hole section in K-01 Well was in the outside of the constructed GLRW therefore loss circulation problem occurred. The recommended gas-liquid rate combination from this research can be used to determine the gas-liquid rate combination to prevent loss circulation problems, wellbore damage and cutting transport problems.
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