用风暴节流阀代替失效的TRSCSSV维持高产气井的生产

Hanani Zaidil
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引用次数: 0

摘要

1A井是一口高产的大口径干气井,由于该井的液压控制管线出现故障,安装了风暴节流阀。由于其试点实施,为期一年的试验期被强制执行,作为阀门耐久性和可靠性测试的一部分。本文的目的是展示在为期一年的试验期结束后观察到的阀门无意关闭(在FTHP高于阀门设定压力时跳闸)的根本原因分析的结果,该结果已经显示出98%的可靠性。对三个独立的风暴节流阀进行了物理检查,分析了在五个月内过早关闭的问题,以找到共同的根本原因。研究人员将井参数与已知的操作包线进行了对比,以缩小可能导致意外关闭的井内自然发生或外部诱发的可能性。根据现有数据,引发井下压力和温度数据采集的根本原因仍然是暂时的。对回收阀门的检查发现了常见的损坏元件;活塞o形环。o形圈被发现不是漏水、断裂就是变平了。在分析井参数时,自安装阀门以来检测到的唯一显著变化是井口温度上升了6摄氏度。然而,这种温度的升高不应该影响o型圈的工作包线。该井的完井设计是在射孔上方约2000英尺处使用井下测量仪,以消除电缆测量的需要。这限制了验证油管中预测温度分布的能力。由于怀疑意外关闭与温度有关,因此开展了井下温度测量,以调查其对阀门的影响。根据调查,与模型估计相比,在风暴节流阀深度处记录到的温度要高得多。这为风暴窒息过早关闭问题提供了结论性叙述的关键。较高的温度无意中增加了风暴节流阀的穹顶充注压力,导致阀门在运行时发生物理节流,从而导致密封损坏。考虑到新的穹顶设置压力需要更高的温度,同样性质的意外关闭不再被观察到。这一经验将为未来管理具有风暴节流井的最佳实践提供指导,并概述了监控参数、监控要求、压力设置确定实践、阀门功能测试程序以及阀门在井和场中的处理的建议。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Sustaining Production in a Prolific Gas Well Using Storm Choke in Place of Failed TRSCSSV
Well 1A is a prolific, big bore dry gas well that has been installed with storm choke due to failure of the well's hydraulic control line. Because of its pilot implementation, a one-year trial period was enforced as part of the valve's endurance and reliability test. The objective of this paper is to show findings from a root cause analysis on valve inadvertent closure (trip at FTHP above valve setting pressure) observed after the conclusion of the one-year trial period which had already indicated positive results with 98% reliability. Physical inspection of three separate sets of storm choke that had premature closure issues within a duration of five months were analyzed to find a common root cause. The well parameters were studied versus the known operating envelope to narrow down possibilities that were either naturally occurring or externally induced within the well that could have caused the inadvertent closures. Based on the available data, the root cause remained tentative triggering the need for downhole pressure and temperature data acquisition. Inspections of the retrieved valves revealed common damaged element; the piston O-ring. The O-rings were found to be either leaking, broken or flattened. When analyzing the well parameters, the only significant change detected since the valve installation was the wellhead temperature which had shown increase of 6 degrees Celsius. However, this increase in temperature should not have impacted O-ring's operating envelope. The well was designed to be completed with downhole gauge at approximately 2000 feet above top of perforations to eliminate need for wireline surveys. This limits the ability to verify predicted temperature profile in the tubing. Suspecting the inadvertent closures to be related to temperature, downhole temperature survey was launched to investigate its impact on the valve. Based on the survey, a much higher temperature was recorded at the storm choke valve depth compared to model estimation. This provided the key to provide a conclusive narrative to the storm chokes’ premature closure issues. The higher temperature had inadvertently increased the storm choke's dome charging pressure resulting in physical throttling of the valve when in operation and thus resulting in damaged seals. With the higher temperature being taken into consideration for new dome setting pressure, inadvertent closures of the same nature were no longer observed. This experience will be able to provide a guideline on best practices in managing wells with storm chokes in the future and outline recommendations for parameters to monitor, surveillance requirements, pressure setting determination practices, procedures for valve function testing and valve handling the well and at the yard.
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