{"title":"卤水加热器外壳在焊接处断裂","authors":"","doi":"10.31399/asm.fach.process.c0048733","DOIUrl":null,"url":null,"abstract":"\n The brine-heater shell in a seawater-conversion plant failed by bursting along a welded joint connecting the hot well (C70600 per ASTM B 466) to the heater shell (ASTM A285, grade C steel). Three cracks in the welded joints between the heater shell and the hot well were revealed by visual inspection. It was observed that crack 1 and 2 were covered with high-temperature oxidation products which revealed that the surfaces had been separated for quite some time. A very high discontinuity stress which existed at the longitudinal welds between the hot well and the heater shell was revealed by stress analysis. It was interpreted that the cracks had originated shortly after the heater was put into operation and propagated slowly initially. The rate of propagation was interpreted to have increased due to discontinuity stresses greater than yield strength of the material. It was concluded that the brine heater cracked and fractured because it was overstressed in normal operation. The heater design was modified to make the heater shell and the hot well two separate units. A relief valve was recommended in the heater or in the steam line near the heater.","PeriodicalId":294593,"journal":{"name":"ASM Failure Analysis Case Histories: Processing Errors and Defects","volume":"79 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Fracture of a Brine-Heater Shell at Welds\",\"authors\":\"\",\"doi\":\"10.31399/asm.fach.process.c0048733\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"\\n The brine-heater shell in a seawater-conversion plant failed by bursting along a welded joint connecting the hot well (C70600 per ASTM B 466) to the heater shell (ASTM A285, grade C steel). Three cracks in the welded joints between the heater shell and the hot well were revealed by visual inspection. It was observed that crack 1 and 2 were covered with high-temperature oxidation products which revealed that the surfaces had been separated for quite some time. A very high discontinuity stress which existed at the longitudinal welds between the hot well and the heater shell was revealed by stress analysis. It was interpreted that the cracks had originated shortly after the heater was put into operation and propagated slowly initially. The rate of propagation was interpreted to have increased due to discontinuity stresses greater than yield strength of the material. It was concluded that the brine heater cracked and fractured because it was overstressed in normal operation. The heater design was modified to make the heater shell and the hot well two separate units. A relief valve was recommended in the heater or in the steam line near the heater.\",\"PeriodicalId\":294593,\"journal\":{\"name\":\"ASM Failure Analysis Case Histories: Processing Errors and Defects\",\"volume\":\"79 1\",\"pages\":\"0\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2019-06-01\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"ASM Failure Analysis Case Histories: Processing Errors and Defects\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.31399/asm.fach.process.c0048733\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"ASM Failure Analysis Case Histories: Processing Errors and Defects","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.31399/asm.fach.process.c0048733","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
摘要
海水转换厂的盐水加热器外壳由于连接热井(ASTM B 466 C70600)和加热器外壳(ASTM A285 C级钢)的焊接接头爆裂而失效。通过目测发现,加热器壳体与热井焊缝处有3处裂纹。观察到裂纹1和裂纹2被高温氧化产物覆盖,表明裂纹表面已分离相当长时间。应力分析表明,热井与加热器壳体之间的纵向焊缝处存在很高的不连续应力。分析认为,裂纹是在加热炉投入运行后不久产生的,最初扩展缓慢。传播速率被解释为由于大于材料屈服强度的不连续应力而增加。分析认为,卤水加热器在正常运行过程中受力过大,导致其开裂断裂。对加热器的设计进行了改进,使加热器壳体和热井成为两个独立的单元。建议在加热器或加热器附近的蒸汽管道上安装安全阀。
The brine-heater shell in a seawater-conversion plant failed by bursting along a welded joint connecting the hot well (C70600 per ASTM B 466) to the heater shell (ASTM A285, grade C steel). Three cracks in the welded joints between the heater shell and the hot well were revealed by visual inspection. It was observed that crack 1 and 2 were covered with high-temperature oxidation products which revealed that the surfaces had been separated for quite some time. A very high discontinuity stress which existed at the longitudinal welds between the hot well and the heater shell was revealed by stress analysis. It was interpreted that the cracks had originated shortly after the heater was put into operation and propagated slowly initially. The rate of propagation was interpreted to have increased due to discontinuity stresses greater than yield strength of the material. It was concluded that the brine heater cracked and fractured because it was overstressed in normal operation. The heater design was modified to make the heater shell and the hot well two separate units. A relief valve was recommended in the heater or in the steam line near the heater.