油井寿命设计:优化UGS井的水泥封堵质量

Fei Gao, Rui Wang, Hongsheng Su, S. Zhong, Yabin Guo, S. Taoutaou
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引用次数: 1

摘要

在一个29口地下储气库(UGS)项目的施工过程中,开发了一种设计方法来获得最佳环空水泥屏障,以最大限度地延长UGS井在随后的生产状态下的寿命。该方法的有效性得到了该项目投产后多年来所有井的地面和地下数据的验证。UGS井毗邻居民区,因此可靠的井完整性具有重要意义。为了实现这一目标,为整口井准备了固井设计,以获得良好且持久的层间隔离。设计的重点是井的长期完整性和寿命,而不是短期效益。首先,回顾了固井技术,以便在该项目中应用高质量固井作业的最佳实践。其次,采用先进的第三界面脉冲回波固井评价测井工具,以便更好地了解固井效果,并将其用于后续的工作改进。该工具测量环空材料和套管间隙的状态,这对固井质量有很大影响。第三,引入了具有工程机械性能的高性能柔性/可膨胀(HPFE)水泥体系。通过专门的水泥应力模拟软件,优化了水泥的力学性能,以应对完井和生产过程中水泥所面临的井下压力和温度变化。预计温度变化在69℃至81℃之间波动,压力在17 MPa至34 MPa之间波动。从UGS井的5年生产中,记录了井下温度和压力。压力值在预测范围内。温度比预期的要高,但设计的水泥凝块足够坚固,可以应对更高的温度。从2011年到2016年,共有29口UGS井被固井。由于通过优化作业方案的迭代不断努力提高固井质量,项目后4年固井胶结测井结果优于前2年。2013年6月,部分井投产,开始注气。在接下来的5年里,整个存储区块逐步投入生产,达到满负荷生产。根据过去5年的现场数据和水泥固井力学性能,我们进行了作业后水泥完整性数值研究。结果表明,在各种井下条件下,水泥屏障都能保持完整。作业后的生产行为证明了这一点,在注气和抽气周期中对生产行为进行了监测,在此过程中没有报告持续套管压力(SCP)问题。固井方案的设计从一开始就关注井眼质量,目的是通过持久的井完整性来最大化井眼寿命。基于每个作业设计-执行-评估周期的设计迭代有助于提高整个项目的固井质量。最佳实践实施、可靠的固井胶结评估工具和设计的HPFE固井系统相结合,实现了井的坚固完整性。作业后连续的井下和地面数据采集证明了这种持久的油井完整性。此次收购还对同一区块未来UGS井的井下动态预测模型进行了微调,为工程HPFE水泥系统设计提供了更现实的开始。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Design for Well Longevity: Optimizing Cement Barrier Quality in UGS Wells
A design approach was developed to obtain an optimum annulus cement barrier during well construction of a 29-well underground gas storage (UGS) project to maximize the longevity of the UGS wells in the years that followed in production state. The effectiveness of this approach was verified by multi-year post-job surface and subsurface field data from all the wells from the time the wells were put into production in this project. The UGS wells are adjacent to a residential area, making reliable well integrity of great significance. To facilitate this, the cementing design for an entire well was prepared to obtain good and durable zonal isolation. The design focused on long-term well integrity and longevity rather than short-term effectiveness. First, the cementing technique was reviewed so that best practice for a high-quality cementing operation was applied in this project. Second, an advanced third-interface pulse-echo cement evaluation logging tool was adopted for better understanding of the cementing job results and to use the indications for subsequent job improvement. The tool measures the state of annulus material and casing standoff, which considerably impacts the cementing quality. Third, a high-performance flexible/expandable (HPFE) cement system with engineered mechanical properties was introduced to the project. With a specialized cement stress simulation software, the mechanical properties of the cement were optimized to deal with the downhole varying pressures and temperatures the cement would see during completion and production. Temperature change was predicted to fluctuate between 69 and 81°C and pressure between 17 MPa and 34 MPa. From the 5 years of production of the UGS wells, downhole temperature and pressure were recorded. Pressure values were within the predicted range. The temperature was higher than expected, but the designed set cement was robust enough to deal with the higher temperature. In all, 29 UGS wells were cemented from 2011 to 2016 in this campaign. Due to the continuous effort of improving the cementing quality through the iterations of optimizing job program, the cement bond log result was better in the later 4 years of the project compared to the first 2 years. In June 2013, some of the wells were put into production and gas injection initiated. In the following 5 years, the whole storage block was gradually put into production up to its full capacity. We conducted a post-job numerical cement integrity study based on the acquired field data from the last 5 years with the measured set-cement mechanical properties. The result indicates the cement barrier can remain intact under the varying downhole conditions. This is evidenced by the post-job production behavior, which was being monitored during the gas injection and withdrawal cycles and no sustained casing pressure (SCP) problem was ever reported during the process. The design for the cementing program focused on the well barrier quality from the beginning with the goal of maximizing well longevity by means of a durable well integrity. The design iterations based on a job-by-job design-execute-evaluate cycle helps improve the cement job quality throughout the whole project. The combination of best practice implementation, reliable cement bond evaluation tool, and the engineered HPFE cement system realized a robust well integrity for the wells. This lasting well integrity is evidenced by continuous post-job downhole and surface data acquisition. The acquisition also fine-tuned the model for predicting downhole dynamics for future UGS wells in the same block, facilitating a more realistic start for the engineered HPFE cement system design.
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