北非盆地压裂行动的优化

Aly Rasyid
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引用次数: 1

摘要

钻井优化的目标是降低成本,改善井眼条件和油藏的完整性,同时建立最大的安全性能和环境监管。尽管钻井作业的最终结果很容易观察到,但几乎总是被忽视的是,钻井作业的规划和执行所涉及的问题的复杂性,以及这一过程中涉及的主题的数量。本文以北非滨田地区勘探钻井为例,对其进行了评价。在2006年至2011年期间,实现了持续的钻井改进。优化的关键要素包括管理钻井团队结构、工程井规划、改进钻井作业管理(如现场安全管理实践),以及钻后分析,以便为下一口井提供经验教训。结果,在2006年至2011年期间,共钻了26口井,成功地将钻井时间从87天(第一口井)减少到平均40天,并取得了良好的安全记录。关键词:优化,钻井成本,钻井性能
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Optimisasi Operasi Pemboran Di Basin Afrika Utara
Drilling optimization objective was to reduce costs, improve wellbore conditions and integrity for increasingly challenging reservoirs while establishing maximum safety performance and environmental custodianship. Even though the final result of a drilling operation is easily observed, what almost always goes unnoticed is the complexity of the issues involved in the planning and execution of a drilling operation and the number of topics involved in such a process. In this paper, as case study of the exploration drilling in Hamada region, North Africa has been evaluated. Over the period of 2006 to 2011, continued drilling improvement was achieved. Key elements in the optimization included focus on management drilling team structure, engineering well planning, improvements on managing drilling operations such as on site safety management practices, and also post drill analysis to implement lesson learn for the next well to be drilled. As the result, while drilling 26 wells during the 2006 until 2011, drilling days were successfully reduced from 87 days (first well) to the average 40 days, and very good safety record performance. Keywords : optimization, drilling cost, drilling performance
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