拉法基白厅工厂的电力成本降低措施

M. Rose
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引用次数: 5

摘要

1991年,宾夕法尼亚州东部的水泥公司受到经济不景气和市场竞争激烈的影响。拉法基白厅工厂也不例外,并努力通过降低成本来提高利润。对企业和水泥行业成本的严格分析表明,与行业标准相比,工厂的电力成本过高。事实上,该工厂的电力成本是所有拉法基北美工厂中最高的。本文介绍了成本节约措施的历史和效果。确定需要改进的两个主要领域是电力合同和电力利用效率。该厂于1992年开始与宾夕法尼亚州电力和照明公司(PP&L)进行电力合同谈判,并于当年8月签订了一份新的可中断电力合同。该合同保证了较低的需求和能源费率,但却使客户受到限电的影响。有了可中断合同,分析了合同的各个组成部分,以节省额外的成本。采取的主要措施包括优化生产计划和在高峰时段谨慎使用生产设备。1995年安装了柴油发电机,以便在停电期间提供替代能源,减轻公用事业公司保证昂贵的稳定需求水平的负担。结果,1996年工厂的电力成本比1991年的成本降低了40.6%。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Power costs reduction measures at Lafarge Whitehall plant
In 1991, the cement companies in eastern Pennsylvania suffered from a poor economy and strong competition within the marketplace. The Lafarge Whitehall plant was no exception and endeavored to become more profitable through cost reduction. Rigorous analysis of both corporate and cement industry costs revealed that the plant power costs were excessive compared to industry standards. In fact, the plant had the highest power costs of all Lafarge North American plants. This paper gives a history of cost saving measures and results thereof. The two major areas identified for improvement were the power contract and power utilization efficiency. The plant initiated power contract negotiations with Pennsylvania Power and Light Company (PP&L) in 1992, which concluded with a new interruptible power contract in August of that year. The contract guaranteed lower demand and energy rates, yet subjected the customer to power curtailments. With the interruptible contract in place, the various components of the contract were analyzed for additional cost savings. Primary measures taken included production schedule optimization and careful utilization of production equipment during on-peak hours. Diesel generators were installed in 1995 to provide an alternate source of power during curtailments, lessening the burden on the utility to guarantee costly firm demand levels. As a result, the 1996 plant power costs were reduced by 40.6% from 1991 costs.
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