掺合料对B-1混凝土工程坍落度减小和混凝土抗压强度的影响

B. S. Budi, S. ., E. Suhartono, M. -, Sukoyo -, Bintang -, Sakdiyah -
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摘要

三宝垄-索罗收费公路是跨爪哇高速公路的一部分,对道路网络的发展具有战略意义,特别是在爪哇中部和区域范围内。建设工程一般由开挖、堆垛和桥梁工程组成。因此,项目中的工作数量可能会出现一个阻碍开发过程的问题,其中一个问题与Kali Putih 1号桥建设中的混凝土浇筑有关,其中P1和P3柱的混凝土浇筑坍落度下降(30 Mpa)。然而,在STA的P1柱上进行了坍落度试验。61 + 368,500, STA中的P3。61 + 293500,分别造成3.5 cm和4 cm的塌陷。因此,它们不符合B-1混凝土的规范,即7.5±2.5 cm。此外,使用高效减水剂来克服这个问题,因为它能够恢复新鲜度/可加工性。因此,本研究旨在通过压力试验,确定掺入高效减水剂和缓凝剂对混凝土抗压强度、坍落度降低和时间的影响,利用24个圆柱形试件(7天和14天)进行试验。在120分钟内,每隔20分钟进行一次坍落度测试,以确定减凝时间,结果进一步表明,在B-1类混凝土中添加缓凝剂能够延长其功能期(坍落度为7±2.5 cm时,功能期为67分钟)。然而,加入高效减水剂也能修复不符合要求的坍落度,包括加入缓凝剂(82.5分钟)的试样,导致坍落度从1.9 cm增加到17.5 cm,增加后进一步增加。此外,这些影响是由于其在7天和14天的试件上分别降低了3.13%和6.14%的抗压强度。但SPSS v.23.0检验结果显示,普通混凝土+缓凝剂与普通混凝土+缓凝剂+ SP抗压强度差异,sig值为0.021
本文章由计算机程序翻译,如有差异,请以英文原文为准。
The Effects of Admixtures Addition on Slump Decrease and Concrete Compressive Strength at B-1 Concrete Works
Semarang - Solo Toll Road is part of the Trans Java highway, which has a strategic meaning in the development of road networks, specifically in Central Java and also on a regional scale. The construction project generally consists of excavation work, stockpiles and bridge work. The number of work in the project therefore allows the emergence of a problem that can hinder the development process and one of which was related to concrete casting in the construction of the Kali Putih Bridge 1, where there was a slump decrease in columns P1 and P3 concrete pre-casting (30 Mpa). However, a slump test was carried out on column P1 in STA. 61 + 368,500, and P3 in STA. 61 + 293,500, which resulted in 3.5 cm and 4 cm collapse respectively. Hence, they did not meet specification on B-1 concrete, which was 7.5 ± 2.5 cm. In addition, Superplasticizer was used to overcome this problem, as it was capable of restoring freshness/workability. This study, therefore, aimed to determine the effect of the incorporating superplasticizer and retarder into concrete, on its compressive strength, slump decrease, and time, utilizing 24 test cylindrical specimens (7-days and 14-days), through pressure testing. Furthermore, the slump testing was conducted every 20 minutes for 120 minutes, to determine the reduction time, and the findings further indicated that adding a retarder to class B-1 concrete was capable of increasing the functional period (67 minutes on a slump of 7 ± 2.5 cm). However, the addition of Superplasticizer was also able to repair the slumps, which did not meet the requirements, including the specimen that involved the incorporation of a retarder (82.5 minutes, which resulted in a 1.9 cm slump that was further increased to 17.5 cm after augmentation. Furthermore, these effects were due to its ability to reduce the compressive strength by 3.13% and 6.14% on the 7-days and 14-day specimens, respectively. However, the SPSS v.23.0 test results showed the difference in compressive strength between the normal concrete + retarder and normal concrete + retarder + SP, with a sig value of 0.021
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