由于热影响区螺纹根部裂纹导致的节流臂总成失效

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引用次数: 0

摘要

飞机发动机的节流阀臂断裂,导致发动机失去控制。断裂的部分由6.4毫米(1/4英寸)直径的中碳钢杆组成,带有一根螺纹,用于安装插入节气门旋钮的滚花黄铜螺母。螺纹杆被焊接到节流阀连杆上,通过在螺纹部分附近的连杆上进行组装焊沉积。断口呈粗粒脆性组织,在螺纹根部有起裂。由于相邻焊层热影响区内螺纹根部存在裂纹,导致节流阀臂发生脆性断裂。焊接热产生的铁素体晶界网络较弱的粗晶组织没有通过焊后热处理加以纠正。裂纹和这种不利的微观结构的结合提供了一个弱化的条件,导致在正常的施加载荷下发生灾难性的脆性断裂。设计被改变,以消除焊接邻近的螺纹部分的杆。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure of a Throttle-Arm Assembly Because of Thread-Root Cracks in the HAZ
A throttle arm of an aircraft engine fractured and caused loss of engine control. The broken part consisted of a 6.4-mm (1/4-in.) diam medium-carbon steel rod with a thread to fit a knurled brass nut that was inserted into the throttle knob. The threaded rod had been welded to the throttle-linkage bar by an assembly-weld deposit made on the rod adjacent to the threaded portion. The fracture surface exhibited a coarse-grain brittle texture with an initiating crack at a thread root. The throttle-arm failed by brittle fracture because of the presence of cracks at the thread roots that were within the HAZ of the adjacent weld deposit. The heat of welding had generated a coarse-grain structure with a weak grain-boundary network of ferrite that had not been corrected by postweld heat treatment. The combination of the cracks and this unfavorable microstructure provided a weakened condition that resulted in catastrophic, brittle fracture under normal applied loads. The design was altered to eliminate the weld adjacent to the threaded portion of the rod.
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