{"title":"基于自动优化AGC煤量预测控制方法的研究与应用","authors":"Xiaogang Xin, Shaojia Dang, Cheng-guo Qin, Guopeng Zhang, Rui Guo","doi":"10.2991/MASTA-19.2019.39","DOIUrl":null,"url":null,"abstract":"One circulating fluidized bed boiler (CFB) generator set of a thermal power plant in Inner Mongolia power grid planned to put into automatic power generation control (AGC) by transforming the software and hardware of the unit. This can reduce the electricity allocation and punishment by the power grid. In order to overcome the characteristics of large delay and inertia of CFB unit and improve the quality of AGC, a multi-feedforward is added to the boiler master, the prediction section and configuration of coal quantity were designed, and a new objective function was devised to self-optimize the coal quantity. Logic of automatic optimization was made to improve the control indexes of AGC. After the AGC test was finished and AGC was put into operation, the indexes of AGC are excellent, which not only eliminates the AGC power punishment, but also obtains the reward.","PeriodicalId":103896,"journal":{"name":"Proceedings of the 2019 International Conference on Modeling, Analysis, Simulation Technologies and Applications (MASTA 2019)","volume":"22 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-07-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Research and Application of Prediction Control Method Based on Automatic Optimization of Coal Volume in AGC\",\"authors\":\"Xiaogang Xin, Shaojia Dang, Cheng-guo Qin, Guopeng Zhang, Rui Guo\",\"doi\":\"10.2991/MASTA-19.2019.39\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"One circulating fluidized bed boiler (CFB) generator set of a thermal power plant in Inner Mongolia power grid planned to put into automatic power generation control (AGC) by transforming the software and hardware of the unit. This can reduce the electricity allocation and punishment by the power grid. In order to overcome the characteristics of large delay and inertia of CFB unit and improve the quality of AGC, a multi-feedforward is added to the boiler master, the prediction section and configuration of coal quantity were designed, and a new objective function was devised to self-optimize the coal quantity. Logic of automatic optimization was made to improve the control indexes of AGC. After the AGC test was finished and AGC was put into operation, the indexes of AGC are excellent, which not only eliminates the AGC power punishment, but also obtains the reward.\",\"PeriodicalId\":103896,\"journal\":{\"name\":\"Proceedings of the 2019 International Conference on Modeling, Analysis, Simulation Technologies and Applications (MASTA 2019)\",\"volume\":\"22 1\",\"pages\":\"0\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2019-07-01\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"Proceedings of the 2019 International Conference on Modeling, Analysis, Simulation Technologies and Applications (MASTA 2019)\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.2991/MASTA-19.2019.39\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"Proceedings of the 2019 International Conference on Modeling, Analysis, Simulation Technologies and Applications (MASTA 2019)","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.2991/MASTA-19.2019.39","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
Research and Application of Prediction Control Method Based on Automatic Optimization of Coal Volume in AGC
One circulating fluidized bed boiler (CFB) generator set of a thermal power plant in Inner Mongolia power grid planned to put into automatic power generation control (AGC) by transforming the software and hardware of the unit. This can reduce the electricity allocation and punishment by the power grid. In order to overcome the characteristics of large delay and inertia of CFB unit and improve the quality of AGC, a multi-feedforward is added to the boiler master, the prediction section and configuration of coal quantity were designed, and a new objective function was devised to self-optimize the coal quantity. Logic of automatic optimization was made to improve the control indexes of AGC. After the AGC test was finished and AGC was put into operation, the indexes of AGC are excellent, which not only eliminates the AGC power punishment, but also obtains the reward.