克服马来西亚第一个深水气田的流动保障挑战

Suphawat Kiertkul, K. Saranyasoontorn
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引用次数: 0

摘要

H区块位于Sabah近海水深1300米处,由Rotan和Buluh油田组成。安装完海底采油树、跳管、管汇、脐带缆、立管和流动管线后,将其回接到FLNG设备上。该项目的目标是开发最实用和有效的解决方案,以克服由于海底温度低和高压气体造成的流动保证挑战,从而从马来西亚第一个深水气田获得第一次天然气。在OLGA软件中建立了一个具有所有现场条件的模型,用于模拟和预测海底井、立管、管线以及上层设施的每个关键点的工艺参数。此外,从海底井、跳线、立管和管线一直到上层进口接收设施的所有限制条件都经过仔细审查和优化,并谨慎地确定了分步方法,即利用井中的高压气体从管线中移除约1000立方米预充的MEG流体,称为“DeMEG操作”,然后将气体输送到LNG工艺操作中。由于深水气井的压力为200-230 bar,海底温度为2-4°C,加上储层含水层提供的饱和气中已有的含水量,因此预计该作业将在水合物区进行。不可避免的潜在后果之一是水合物的形成,并可能导致跳线、立管甚至流管的堵塞。DeMEG作业结果表明,由于冷启动过程中的焦耳-汤普森冷却,水下节流阀下游的最低温度为- 23°C。一种缓解策略是在海底井口注入一批MeOH,直到温度高于水合物点。当气体沿着管线流动后,在稳定状态下,它会冷却到海底的温度。因此,额外的缓解措施是连续注入单乙二醇(MEG)作为另一种与气流混合的热力学水合物抑制剂。MEG附着水分子,从而阻止它们在气体分子周围形成一个笼子,以防止水合物的形成。为了克服上层的液体处理能力,该公司精心规划了多阶段的DeMEG作业,并最终在海上进行,直到流水线上剩余的MEG达到合理可行的水平,才能继续从油田生产天然气。在团队的出色合作和合理规划下,DeMEG解决方案以及水合物减缓策略被证明是有效的,并且调试操作按照计划成功完成,直到21年2月6日第一次天然气获得并供应给FLNG。7天后,第一次液化天然气下降。该油田为PTTEP及其合资伙伴增加了约2.7亿立方英尺/天的产量,相当于每天45,000桶石油。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Overcoming Flow Assurance Challenges of the First Deepwater Gas Field in Malaysia
Block H, located in 1,300 meters of water depth at offshore Sabah, consists of Rotan and Buluh fields. The subsea trees, jumpers, manifold, umbilicals, risers and flowlines were installed and tied-back to an FLNG facility. The objective of this project was to develop most practical and effective solutions to overcome flow assurance challenges owing to low seabed temperature and high-pressure gas to achieve 1st gas from the first deepwater gas field in Malaysia. A model was built in OLGA software with all field conditions to run simulations and predict process parameters at every critical point in subsea wells, risers and flowlines as well as topside facilities. Besides, all constraints from the subsea wells, jumpers, risers and flowlines all the way to topside inlet receiving facilities were carefully reviewed and optimized with an abundance of caution to determine the stepwise approach by utilizing the high-pressure gas from wells to remove around 1,000 m3 of pre-filled MEG fluid out of the flowline, called ‘DeMEG operation’ before feeding gas to LNG process operations. With 200-230 barg pressures from deepwater gas wells and 2-4°C temperature at seabed as well as pre-existing water content in saturated gas given by reservoir aquifer, this start-up operation would expect to be in the hydrate zone. One of the unavoidable potential consequences was a hydrate formation and could result in plugging of jumpers, risers or even flowlines. The DeMEG operation results indicated the lowest temperature at the downstream of the subsea choke was −23°C due to Joule-Thompson cooling during the cold start. One mitigation strategy was to inject a batch of MeOH at the subsea wellhead until the temperature is above the hydrate point. After the gas flowed along the flowlines, it would cool down to the seabed temperature during the steady state condition. Hence, additional mitigation was to continuously inject Mono Ethylene Glycol (MEG) as another thermodynamic hydrate inhibitor mixed with gas stream. The MEG affixed water molecules and thus deterred them from forming a cage around gas molecules to prevent hydrate formation. A multi-stage DeMEG operation was carefully planned to overcome liquid handling capacity at topside and eventually executed at offshore until the remaining MEG in the flowline was as low as reasonably practical to proceed with gas production from the field. With an excellent collaboration from the team and proper planning, the DeMEG solution together with hydrate mitigation strategy were proven to be effective and the commissioning operation was successfully completed as per the plan until the 1st gas was achieved on 6-Feb-21 and supplied to FLNG. The 1st LNG drop subsequently came in 7 days later. This field has increased production volume around 270MMSCFD, equivalent to 45,000 barrels of oil per day to PTTEP and JV partners.
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