氯气生产设备故障的评估

S. Andrew, R. Caligiuri, L. E. Eiselstein, T. K. Parnell
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引用次数: 0

摘要

氯气生产设施的一个过程发生故障,导致泄漏,迫使附近城镇的部分居民撤离。调查显示,事故起因是用于冷凝氯气的管壳式热交换器(液化器)发生故障。事故发生后的检查发现,液化器冷却剂进口处的一块布加速了该区域的流动,导致某些管道破裂。结果,水基卤水液化器冷却剂被夹带在氯工艺流中,形成高酸性氧化混合物。然后,这种腐蚀性混合物流入氯储罐,破坏了储罐入口管道中的弯头,使储罐关闭罐阀失效,从而使氯排放到大气中。本文讨论了用于调查这一事件的多学科方法。特别是,本文讨论了所进行的详细物理检查,用于确定流动条件的有限元分析以及用于评估失效的腐蚀测试。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Evaluation of a Failure in a Chlorine Production Facility
A process upset at a chlorine production facility resulted in a release that forced the partial evacuation of a nearby town. Investigations revealed that the events commenced with the failure of a shell and tube heat exchanger (liquefier) used to condense chlorine gas. Post-incident inspections revealed a cloth at the liquefier coolant inlet that accelerated the flow in that region, causing certain tubes to be breached. As a result, the water-based brine liquefier coolant was entrained in the chlorine process stream, forming a highly acidic oxidizing mixture. This corrosive mixture then flowed to the chlorine storage tanks destroying an elbow in the tank inlet piping and rendering the tank shut-off tank valve ineffective, thus allowing chlorine to vent into the atmosphere. This paper discusses the multi-disciplinary approach used to investigate this incident. In particular, this paper discusses the detailed physical inspections performed, the finite element analyses used to determine the flow conditions, and the corrosion testing conducted to evaluate the failure.
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