电枢制造过程中由于片层撕裂造成的失效

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引用次数: 0

摘要

在对直流电机(4475千瓦或6000马力)的大型电枢进行最后一次车间焊接时,听到一声巨响,焊接工作停止了。当焊缝处于冷态时,无损评价显示根部焊缝附近有一个大裂纹。研究表明,主裂纹沿亚临界热影响区平行于熔合边界扩展,并伴有II型硫化锰(MnS)夹杂物的长串。这支持了以下结论:由于焊缝设计、焊接顺序和热效应在焊缝根部引起的高旋转应变,导致了焊缝的片层撕裂。建议包括将旧焊件移至裂纹以外的深度,并用较软的焊接金属层代替,然后再将主焊缝焊接到较软的金属层上。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Failure During Fabrication of an Armature Because of Lamellar Tearing
During the final shop welding of a large armature for a direct-current motor (4475 kW, or 6000 hp), a loud bang was heard, and the welding operation stopped. When the weld was cold, nondestructive evaluation revealed a large crack adjacent to the root weld. Investigation showed the main crack had propagated parallel to the fusion boundary along the subcritical HAZ and was associated with long stringers of type II manganese sulfide (MnS) inclusions. This supported the conclusion that the weld failed by lamellar tearing as a result of the high rotational strain induced at the root of the weld caused by the weld design, weld sequence, and thermal effects. Recommendations included removing the old weldment to a depth beyond the crack and replacing this with a softer weld metal layer before making the main weld onto the softer layer.
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