在泰国海上的连续油管上,首次使用新设计的试验磨铣钻头,在小井眼井中进行了非常窄间隙的永久油管贴片磨铣

Monchai Nimsuk, Treepun Tipapong, Surapong Somjai, Thanawee Kreethapon, Nophadol Jiemsawat, Tuanangkoon Daohmareeyor, Arweephan Kangsadarn, Reawat Wattanasuwankorn, Prapas Phayakrangsee
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引用次数: 0

摘要

永久油管贴片是一种广泛应用于隔离产水层的主要方法,特别是在小井眼中。顾名思义,永久油管贴片是一种不可回收的设备,在需要拆除时带来了很大的挑战。在全球范围内,没有任何记录表明在小井眼中安装永久性油管补丁是成功的。本文将讨论在小井中首次实现连续油管(CT)磨铣永久油管补丁的方法。选择连续油管传送BHA,铣削油管补丁密封段。偏心导铣钻头(外径为2.780 in)经过精心设计,因为它需要通过井下安全阀(DHSV)的内径限制(2.813 in),同时仍然能够剥离油管补片密封内径(2.250 in),直到达到油管内径(2.992 in)的完整进尺,并确保在磨铣过程中不会损坏管壁。一旦移除油管补丁密封段,就会进行编织线(WL)作业,将油管补丁体拉出并收回到地面。随后对该井进行了修复,以进行进一步的干预和生产。连续油管完美地完成了磨铣作业,精心设计的地面设备堆叠设计为连续油管和WL修井提供了井下工具部署的可及性和便利性。在磨铣深度以上的几个衰竭层,将硝化液与连续油管一起使用,以减轻漏失问题。最终,在不破坏油管完整性的情况下,成功磨铣了油管贴片密封。一旦油管补丁密封元件被成功移除,补丁体变得自由,WL就会通过CT堆下入油管补丁体。这是第一次在不损坏一次完井的情况下,以这种方式将永久油管补丁移除并回收到地面。它的成功源于经过深思熟虑的钻头设计和精心的执行。该案例研究现在可以在整个行业中分享,以提高修井效率,并最大限度地减少由于永久性油管补丁移除问题而导致的早期桥塞和弃井的可能性。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
The First Application of Permanent Tubing Patch Milling With Very Narrow Clearance in a Slimhole well with a Newly Engineered Pilot Mill Bit Design for Coiled Tubing, Offshore Thailand
The permanent tubing patch is a primary method widely used to isolate water production zones, especially in slim-hole wells. As the name implies, the permanent tubing patch is non-retrievable equipment and presents a significant challenge when removal is needed. None of the global records of permanent tubing patches installed in slim-hole wells demonstrate successful removal. This paper will discuss the methods used to achieve the first-ever Coiled Tubing (CT) milling of a permanent tubing patch in a slim-hole well. CT was selected to convey the BHA for milling the tubing patch sealing section. An eccentric pilot milling bit (2.780 in OD) was carefully designed as it needed to pass an ID restriction (2.813 in) in the Downhole Safety Valve (DHSV) while still being able to peel off the tubing patch sealing ID (2.250 in) until reaching the full drift of tubing ID (2.992 in) and ensure that the tubing wall would not be damaged during the milling operation. Once the tubing patch sealing section was removed, a braided-line (WL) operation was run to pull free and retrieve the tubing patch body to surface. The well was then restored to enable further intervention and production. CT performed the milling operation flawlessly, and a carefully designed surface equipment stack-up design provided downhole tool deployment accessibility and convenience for both CT and WL intervention. Nitrified fluid was used with CT to mitigate loss problems in several depleted zones above the milling depth. As a result, the tubing patch seal was successfully milled without jeopardizing the tubing integrity. Once the tubing patch seal element was successfully removed and the patch body became free, the WL was deployed through the CT stack to fish the tubing patch body. This is the first-ever operation to remove and retrieve a permanent tubing patch to the surface in this way without damaging the primary completion. Its success results from a well-thought-out pilot mill bit design and careful execution. This case study can now be shared across the industry to improve intervention efficiency and minimize the chance of early plug and abandonment due to permanent tubing patch removal issues.
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