飞机部件的腐蚀开裂

Jivan B. Shah
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引用次数: 0

摘要

2000-T6铝合金托架在沿海环境中失效,原因是腐蚀性氯化物进入了托架和连接螺栓之间。该部件所用材料在使用条件下易受应力腐蚀。铝合金支架与钢螺栓之间的电偶作用可能加剧了开裂。为了防止或尽量减少再次发生,使用中的管件应定期用染料渗透剂检查端面和管件孔内的开裂迹象,并涂上适当的涂层以防止损坏的氯化物。此外,2000-T6铝合金旋转接头由于应力加速腐蚀而发生晶间腐蚀断裂。腐蚀开始是因为铝旋转接头和钢管组件之间的配合松动,导致微动。不适当的维护和/或不正常的维修操作可能会使管件松动。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Corrosion Cracking of Aircraft Components
A 2000-T6 aluminum alloy bracket failed in a coastal environment because corrosive chlorides got between the bracket and attachment bolt. The material used for the part was susceptible to stress corrosion under the service conditions. Cracking may have been aggravated by galvanic action between aluminum alloy bracket and steel bolt. To preclude or minimize recurrences, fittings in service should be inspected periodically by dye penetrant for signs of cracking on the end face and within the fitting hole and protected with a suitable coating to exclude damaging chlorides. Also, a 2000-T6 aluminum alloy swivel fitting experienced intergranular corrosion fracture as the result of stress-accelerated corrosion. Corrosion began because of a loose fit between the aluminum swivel fitting and steel tube assembly, which caused fretting. Inadequate maintenance and/or abnormal service operation may have loosened the fitting.
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