直升机主旋翼传动输出轴故障

J. Hutchinson
{"title":"直升机主旋翼传动输出轴故障","authors":"J. Hutchinson","doi":"10.31399/asm.fach.aero.c9001505","DOIUrl":null,"url":null,"abstract":"\n A helicopter had just taken off when there was a loud bang and the engine started to overspeed. After landing and inspection, the transmission was disassembled. It was discovered that the assembly containing the output shaft to the main rotor had failed. The output shaft assembly was made up of two parts: the output shaft with an integral 10 in. diam upper disc at approximately mid-section; and a 10 in. diam lower disc. During manufacture, the lower disc was attached to the output shaft by an electron beam weld. The fracture had a single fatigue initiation site, coincident with the annular zone of remelted material on the inner surface of the disc. In the lower disc, the fracture was also 80% fatigue, but high stress, low cycle in nature and contained multiple initiation sites coincident with an electron beam weld bead. It was concluded that fatigue in the upper disc resulted from the presence of a metallurgical stress concentration caused by the electron weld beam impingement on the inner surface of the upper disc. An Airworthiness Directive was issued, and the manufacturer issued a mandatory service bulletin outlining a periodic inspection for the output shaft assembly.","PeriodicalId":326464,"journal":{"name":"ASM Failure Analysis Case Histories: Air and Spacecraft","volume":"20 1","pages":"0"},"PeriodicalIF":0.0000,"publicationDate":"2019-06-01","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":"{\"title\":\"Helicopter Main Rotor Transmission Output Shaft Failure\",\"authors\":\"J. Hutchinson\",\"doi\":\"10.31399/asm.fach.aero.c9001505\",\"DOIUrl\":null,\"url\":null,\"abstract\":\"\\n A helicopter had just taken off when there was a loud bang and the engine started to overspeed. After landing and inspection, the transmission was disassembled. It was discovered that the assembly containing the output shaft to the main rotor had failed. The output shaft assembly was made up of two parts: the output shaft with an integral 10 in. diam upper disc at approximately mid-section; and a 10 in. diam lower disc. During manufacture, the lower disc was attached to the output shaft by an electron beam weld. The fracture had a single fatigue initiation site, coincident with the annular zone of remelted material on the inner surface of the disc. In the lower disc, the fracture was also 80% fatigue, but high stress, low cycle in nature and contained multiple initiation sites coincident with an electron beam weld bead. It was concluded that fatigue in the upper disc resulted from the presence of a metallurgical stress concentration caused by the electron weld beam impingement on the inner surface of the upper disc. An Airworthiness Directive was issued, and the manufacturer issued a mandatory service bulletin outlining a periodic inspection for the output shaft assembly.\",\"PeriodicalId\":326464,\"journal\":{\"name\":\"ASM Failure Analysis Case Histories: Air and Spacecraft\",\"volume\":\"20 1\",\"pages\":\"0\"},\"PeriodicalIF\":0.0000,\"publicationDate\":\"2019-06-01\",\"publicationTypes\":\"Journal Article\",\"fieldsOfStudy\":null,\"isOpenAccess\":false,\"openAccessPdf\":\"\",\"citationCount\":\"0\",\"resultStr\":null,\"platform\":\"Semanticscholar\",\"paperid\":null,\"PeriodicalName\":\"ASM Failure Analysis Case Histories: Air and Spacecraft\",\"FirstCategoryId\":\"1085\",\"ListUrlMain\":\"https://doi.org/10.31399/asm.fach.aero.c9001505\",\"RegionNum\":0,\"RegionCategory\":null,\"ArticlePicture\":[],\"TitleCN\":null,\"AbstractTextCN\":null,\"PMCID\":null,\"EPubDate\":\"\",\"PubModel\":\"\",\"JCR\":\"\",\"JCRName\":\"\",\"Score\":null,\"Total\":0}","platform":"Semanticscholar","paperid":null,"PeriodicalName":"ASM Failure Analysis Case Histories: Air and Spacecraft","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.31399/asm.fach.aero.c9001505","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

摘要

一架直升机刚起飞,就听到一声巨响,发动机开始超速。着陆和检查后,变速箱被拆卸。人们发现包含输出轴到主转子的组件已经失效。输出轴总成由两部分组成:输出轴与积分10英寸。上阀瓣直径约在中段;还有一个10英寸。下阀瓣直径。在制造过程中,下圆盘通过电子束焊接连接到输出轴上。断裂有一个单一的疲劳起始点,与圆盘内表面重熔材料的环形区域一致。下盘断裂也是80%的疲劳断裂,但本质上是高应力、低周期断裂,且含有多个与电子束焊缝重合的起始点。结果表明,上盘的疲劳是由电子束撞击上盘内表面引起的冶金应力集中引起的。发布了适航指令,制造商发布了强制性服务公告,概述了输出轴总成的定期检查。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
Helicopter Main Rotor Transmission Output Shaft Failure
A helicopter had just taken off when there was a loud bang and the engine started to overspeed. After landing and inspection, the transmission was disassembled. It was discovered that the assembly containing the output shaft to the main rotor had failed. The output shaft assembly was made up of two parts: the output shaft with an integral 10 in. diam upper disc at approximately mid-section; and a 10 in. diam lower disc. During manufacture, the lower disc was attached to the output shaft by an electron beam weld. The fracture had a single fatigue initiation site, coincident with the annular zone of remelted material on the inner surface of the disc. In the lower disc, the fracture was also 80% fatigue, but high stress, low cycle in nature and contained multiple initiation sites coincident with an electron beam weld bead. It was concluded that fatigue in the upper disc resulted from the presence of a metallurgical stress concentration caused by the electron weld beam impingement on the inner surface of the upper disc. An Airworthiness Directive was issued, and the manufacturer issued a mandatory service bulletin outlining a periodic inspection for the output shaft assembly.
求助全文
通过发布文献求助,成功后即可免费获取论文全文。 去求助
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术官方微信