Bearing Failure Analysis on Gearbox Forced Draft Fan at LNG Plant

Q1 Earth and Planetary Sciences
Edward Rangga Pratama, A. F. H. Mukhammad
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引用次数: 1

Abstract

Boilers Forced Draft Fan has a gearbox reducer to reduce speed from steam turbine as a driver and fan as the driven. Based on Predictive Maintenance Group at Machinery and Heavy Equipment Section, it was found that gearbox has high vibration and noise when boilers load on 195 Ton/Hr (Max Load 295 Ton/hr). Vibration Analysis indicates that the source of vibration comes from bearings with peak value 0.572 in/sec at gearbox high speed outboard vertical and 0.593 in/sec at gearbox high speed outboard horizontal (Max Allowance 0.50 in/sec). Lubrication analysis using X-ray Flourescence method, to see wear particle on lubricating oil showed that Tin(Sn) content is very high 203.62 mg/L (maximum allowance for Tin(Sn) at gearbox is 20mg/L), but wear debris are not found in lubricating oil. Gearbox disassembly found that high speed and low speed bearings suffered severe corrosion. Corrosion at bearings are caused by water contamination on lubrication oil, it comes from steam leak due to carbon ring failure at steam turbine which is steam turbine bearing lubrication and gearbox lubrication get into one lubrication system. After Bearings replaced with a new one, vibration analysis shown improved vibration conditions 0.084 in/sec at gearbox high speed outboard vertical and 0.066 in/sec at gearbox high speed outboard horizontal. In conclucion, high vibration and noise at gearbox reducer were caused by bearings failure due to severe corrosion, and water contamination on lubrication oil for gearbox  due to carbon ring failure on steam turbine.
LNG厂齿轮箱抽风机轴承失效分析
锅炉抽风机采用齿轮箱减速器,以汽轮机为驱动,风机为被驱动进行减速。通过机械重装备科预见性维修组的研究,发现锅炉负荷为195吨/小时(最大负荷295吨/小时)时,齿轮箱存在较大的振动和噪声。振动分析表明,振动源来自轴承,齿轮箱高速舷外垂直和齿轮箱高速舷外水平时的峰值分别为0.572 in/sec和0.593 in/sec(最大允许值0.50 in/sec)。采用x射线荧光法对润滑油进行润滑分析,发现润滑油上有磨损颗粒,Tin(Sn)含量非常高,为203.62 mg/L(齿轮箱处Tin(Sn)最大允许量为20mg/L),但润滑油中未发现磨损碎屑。变速箱拆卸发现,高速和低速轴承遭受严重腐蚀。轴承的腐蚀是由于润滑油受到水的污染而引起的,它是由汽轮机碳环失效引起的蒸汽泄漏引起的,汽轮机轴承的润滑与齿轮箱的润滑合二为一。更换新轴承后,振动分析显示振动条件有所改善,齿轮箱高速舷外垂直和齿轮箱高速舷外水平分别为0.084 in/秒和0.066 in/秒。综上所述,齿轮箱减速机的高振动和高噪声是由于轴承严重腐蚀而失效,汽轮机碳环损坏导致齿轮箱润滑油受到水污染造成的。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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来源期刊
Indonesian Journal of Science and Technology
Indonesian Journal of Science and Technology Engineering-Engineering (all)
CiteScore
11.20
自引率
0.00%
发文量
10
审稿时长
16 weeks
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