First Successful Channel Fracturing Job, in the Middle East, Across Darcy-Permeability Sandstone Formation in Challenging Preperforated Liner Disposal Well Proves to be the Optimum Solution for Enhancing Injectivity

A. A. Fawwaz, Rashid H. Al-Obaid, S. Kurniadi, A. M. Khan, Ziad Al Jalal, Z. Zaouali
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Abstract

Produced water is a byproduct of the production cycle that often creates problems for handling and disposal. In Khafji Joint Operation (KJO), thousands of BWPD were being produced every day and disposed of by pumping the water back into the A formation. This formation is sandstone and has a permeability range over one Darcy. To improve the economics of this project, KJO set an injection target rate of 30,000 B/D per well at a maximum of 1,500-psi wellhead injection pressure due to surface facility constraints. Several completion and stimulation methods were selected to enhance the injectivity rate of these disposal wells. A pilot project was conducted to understand the best methods for injector well development. The well was drilled slanted across the reservoir to increase the reservoir contact area. Openhole and preperforated liners with different upper completion tubing sizes (i.e., 5-in. and 7-in. tubing) were compared to set the baseline of injectivity. Coiled tubing matrix acidizing and hydraulic fracturing were performed in this pilot well to enhance the injectivity. In each different methodology, a series of injection and surveillance tools was deployed to quantify the results. Upon completion with the 5-in. tubing, the pilot well could not achieve the target injectivity rate without well stimulation. An improvement after acid stimulation via coiled tubing was observed, although it was not able to achieve the injectivity target. Completing the well with 7-in tubing improved the injectivity rate slightly, but the injection pressure was still relatively high. Finally, and despite the combination of all challenges in this well, the first channel fracturing in a preperforated injector well in the Middle East was successfully performed. The post-fracturing evaluation shows that channel fracturing is the optimal stimulation method, increasing the injectivity index in this well ninefold compared to matrix acidizing. These results suggest that the implementation of effective fracturing design and operations improves the economics of the project. The results also demonstrate the importance of surveillance activities and their analysis to guide the technical decision and technology deployment. To overcome the challenges, a clear and robust workflow and solution execution and surveillance methods were developed. The pilot project illustrates the importance of having the right data to guide decisions and a rigorous QA/QC approach before, during, and after fracturing to achieve successful delivery.
中东地区首个成功的通道压裂作业,在具有挑战性的预射孔尾管处置井中穿过达西渗透率砂岩地层,被证明是提高注入能力的最佳解决方案
采出水是生产循环的副产品,经常会给处理和处置带来问题。在Khafji联合作业(KJO)中,每天生产数千个BWPD,并通过将水抽回A地层进行处理。该地层为砂岩,渗透率范围超过1达西。为了提高该项目的经济效益,由于地面设施的限制,KJO将每口井的注入速度设定为30,000桶/天,井口注入压力最大为1,500 psi。选择了几种完井和增产方法来提高这些处置井的注入率。为了了解注入井开发的最佳方法,进行了一个试点项目。井斜钻过储层以增加储层接触面积。裸眼和预射孔尾管具有不同的上完井油管尺寸(即5-in)。和7。油管)进行比较,以设定注入能力基线。为了提高注入能力,该试验井进行了连续油管基质酸化和水力压裂。在每种不同的方法中,采用了一系列注入和监测工具来量化结果。5-in完井后。如果没有增产措施,该试验井无法达到目标注入速率。通过连续油管进行酸刺激后,虽然无法达到注入能力目标,但效果有所改善。使用7-in油管完成井后,注入速度略有提高,但注入压力仍然相对较高。最后,尽管这口井面临各种挑战,但在中东地区的一口预射孔注入井中成功进行了第一次通道压裂。压裂后评价表明,通道压裂是最佳增产措施,与基质酸化相比,该井的注入能力指数提高了9倍。这些结果表明,实施有效的压裂设计和作业可以提高项目的经济性。结果还证明了监测活动及其分析对指导技术决策和技术部署的重要性。为了克服这些挑战,开发了一个清晰而健壮的工作流以及解决方案执行和监视方法。该试点项目说明了在压裂之前、压裂期间和压裂之后,拥有正确的数据来指导决策和严格的QA/QC方法对于成功交付的重要性。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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