Sand Consolidation Treatment: Durability in an Alternative Primary Sand Control Method for a Marginal Reservoir

Jing Zhi Kueh, Kok Liang Tan, Daevin Dev, Mohana Ramanee Thamilarasu, Syafiqa Abd Wahab, L. Riyanto, S. Hashim, Anandhadhasan Balasandran, T. Kristanto, C. Ramirez, Yee Choy Chen
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Abstract

Field A is mature hydrocarbon producing field located in east Malaysia discovered in 1963. With multistacked reservoirs more than 7,000 ft high, the reservoirs are predominantly friable and unconsolidated, requiring sand exclusion from the beginning. Most of the wells were completed using internal gravel pack (IGP) methods in the main reservoir. Being an aging producing field, many of the main reservoirs have been depleted and watered out, making the wells inactive. There are, however, several shallower marginal reservoirs, which have been bypassed and undeveloped, known as behind casing opportunity (BCO) reservoirs. The challenge is accessibility to this sand prone reservoir, which might require substantial workover operations, and thus higher costs. Remedial options with proven screen completion can be costly and economically difficult to justify. Mid-2020 marks seven and a half years since the application of a single treatment of epoxy resin in an idle well located in Field A as a remedial approach for BCO. The treatment, proven economically attractive by yielding cost savings of USD 5 million compared to the workover option, further supported by rigorous production monitoring, is unequivocally valuable based on the duration of sustained sand-free production, once again providing reassurance in making this solution a reliable sand-control remedial method for marginal reservoirs. It is important to note that the solution considered a range of laboratory data associated with the chemicals that effectively addressed the requirement based on the characteristics typical of this formation. Well test data from 2013 to 2019 supported sand-free production. Despite experiencing an increment of water cut percentages up to 93.29%, the well is still performing at acceptable production rates. The groundwork processes of candidate identification to the execution of converting the well are described, emphasizing technology comparisons applied in terms of resin fluid system type, execution plan, lessons learned, and best practices developed for maximizing the life of a sand-free producer well.
固砂处理:边缘油藏的一种替代性主要防砂方法的耐久性
A油田是位于马来西亚东部的成熟产油油田,于1963年发现。对于高度超过7000英尺的多层储层,储层主要是脆弱和松散的,从一开始就需要排砂。大部分井在主储层采用内部砾石充填(IGP)方法完成。作为一个老化的生产油田,许多主要油藏已经枯竭和水淹,使井处于闲置状态。然而,仍有一些浅层边缘储层未被开发,被称为下套管机会(BCO)储层。挑战在于易出砂油藏的可达性,这可能需要大量的修井作业,因此成本更高。经过验证的筛管完井补救方案可能成本高昂,而且在经济上难以证明其合理性。自2020年中期以来,作为BCO的补救方法,在a油田的一口闲置井中应用了单一的环氧树脂处理方法,至今已有7年半的时间。与修井方案相比,该处理方案节省了500万美元的成本,并得到了严格的生产监测的进一步支持,具有经济上的吸引力,基于持续无砂生产的持续时间,该解决方案无疑具有价值,再次证明了该解决方案是边缘油藏可靠的防砂补救方法。值得注意的是,该解决方案考虑了一系列与化学品相关的实验室数据,这些数据有效地满足了基于该地层典型特征的需求。2013年至2019年的试井数据支持无砂生产。尽管含水率增加了93.29%,但该井的产量仍然可以接受。介绍了候选井识别到改造井实施的基础过程,强调了树脂流体体系类型、执行计划、经验教训和最佳实践方面的技术比较,以最大限度地延长无砂生产井的寿命。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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