Experimental Verification of Electrostatic Precipitator Stable Operation Under Oil and Co-fuel Firing Conditions of a Coal-fired Power Plant

A. Hoang, T. Nguyen, M. Nguyen
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引用次数: 2

Abstract

Electrostatic Precipitators are usually put into service after a complete shut-off of oil supply to the boiler burners of the furnace of a coal-fired power plant. However, such practice may lead to enormous dust concentration in the flue gas (design value is 37.9 g/Nm³ at 50%RO load) and heavy black smoke appearing at the stack outlet during the oil and/or co-fuel firing condition of boiler. To minimize such problem, an experimental study on charging and electrostatic precipitator operation during unit start-up and shut-down was carried out to verify de-dusting performance. It requires the manual control of the secondary voltages to be lower than sparking voltage of 10~15kV in case of oil and/or co-fuel firing condition of boiler. The study results prove that the electrostatic precipitator runs normally with good de-dusting performance (about 56.4 mg/Nm3 at unit start-up and within 31 mg/Nm3 at unit shut-down) and meets the Vietnamese environmental emission requirements as per proposed specified rules. From the study results, it can be predicted that Electrostatic Precipitators (ESP) & Sea-Flue Gas Desulphurization System (FGD) may be kept running during house load operation and run-back modes. Also, with the ESP and FGD running, the coal-fired power plant may not be limited to the loading dispatch at stable loads under co-firing condition below the minimum load of anthracite coal firing as required from power system.
燃煤电厂燃油和共燃料工况下静电除尘器稳定运行的实验验证
电除尘器一般是在燃煤电厂炉膛锅炉燃烧器完全断油后投入使用。然而,这种做法可能导致烟气中粉尘浓度过高(50%RO负荷时设计值为37.9 g/Nm³),并且在锅炉燃油和/或共燃料燃烧状态下烟囱出口出现重黑烟。为了最大限度地减少这一问题,在机组启动和关闭期间进行了充电和静电除尘器运行的实验研究,以验证除尘器的除尘性能。要求在锅炉燃油和/或共燃工况下,人工控制二次电压低于10~15kV的火花电压。研究结果表明,该静电除尘器运行正常,除尘性能良好(机组启动时约56.4 mg/Nm3,机组停机时在31 mg/Nm3以内),符合越南提出的规定规则的环境排放要求。从研究结果可以预测,静电除尘器(ESP)和海上烟气脱硫系统(FGD)在负荷运行和回流运行两种模式下都可以保持运行。同时,随着电除尘器和烟气脱硫的运行,燃煤电厂可以不局限于电力系统要求的低于无烟煤最小燃烧负荷的共烧条件下稳定负荷的负荷调度。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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