Improving Uptime of Sandy Wells with PCPs Through the Application of Self-Optimization Routines

Conny Velazco-Quesada, Luis Vargas, M. Sawafi, A. Busaidi, Hilal Mamari, A. Yahyai, K. Woolsey, B. Montilla
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Abstract

A field trial has been completed in five oil producing wells, completed with progressive cavity pump (PCP) and under sand co-production scheme with the following objectives: Increasing well uptime by eliminating rotor stuck events and extending time between failures,Reducing locked-in potential associated to slow ramp-up process from initial to target offtake,Reducing the need for operator visits to start or adjust well running conditions after station trips, To achieve this, four wells with very premature failures (less than 6-months) were selected for the trial. One fifth well with high level of depletion was also selected. The target for this last application was to check the impact of reducing fluid level safety factor on pump performance. In all wells, PCP well controllers were installed with self-optimization routines that maintained safe fluid levels above the pump intake while adjusting speed for potential sand ingress. Speed ramp-up time was programmed for completion within two days of start up. First, realtime signals were enhanced to monitor all well parameters that could affect performance, such as tubing head pressure (THP) and casing head pressure (CHP). This information was key to manage the actual fluid levels above the pump, even in gassy wells, allowing safety factors to be reduced by 50% without affecting pump performance. Increase in pump run life by 40 to 140% was observed in the four sandy wells selected. No well interventions were required for sand flushing. Ramp-up time was successfully completed within a day of start-up and after two days production at target was stabilized. After trips, it was found that the well started without the need for operators, as long as power supply was restored. Operator visits were only required for power or signal issues to be fixed, but well was safely kept optimized within those periods. Estimated oil production availability increase from this trial is 12% per well per year. This paper presents the main learnings from applying a self-optimization routine in 5 sandy wells and what is important to consider to achieve cost reduction, increase in well uptime and to reduce the need for manual adjustments/field visits.
应用自优化程序提高pcp砂质井的正常运行时间
现场试验已在五口油井中完成,采用渐进式螺杆泵(PCP)完成,并采用联合采砂方案,目标如下:通过消除转子卡死事件和延长故障间隔时间来增加井的正常运行时间,减少与从初始到目标采油过程缓慢相关的锁定潜力,减少操作员在站起下钻后访问启动或调整井运行条件的需要。为了实现这一目标,选择了4口过早失效(少于6个月)的井进行试验。还选择了1 / 5的高枯竭井。最后一次应用的目标是检查降低液位安全系数对泵性能的影响。在所有井中,PCP井控制器都安装了自优化程序,可以保持泵吸入液面的安全液位,同时根据潜在的进砂量调整速度。加速时间被设定为在启动后两天内完成。首先,增强了实时信号,以监测可能影响性能的所有井参数,如油管头压力(THP)和套管头压力(CHP)。这些信息对于管理泵上方的实际液位至关重要,即使是在气井中,也可以在不影响泵性能的情况下将安全系数降低50%。在所选的4口砂井中,泵的运行寿命增加了40%至140%。不需要对井进行干预,即可进行冲砂。在启动的一天内成功完成了爬坡时间,两天后目标产量稳定。起下钻后,发现只要恢复供电,无需操作人员即可启动。只有在电力或信号问题需要修复时,作业者才需要进行访问,但在此期间,井处于安全优化状态。通过此次试验,预计每口井每年可增产12%。本文介绍了在5口砂质井中应用自优化程序的主要经验,以及为了降低成本、增加正常运行时间和减少人工调整/现场访问的需要,需要考虑的重要因素。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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