The Synthesis and Application of a New Plugging Inhibitor PAS-5 in Water-Based Drilling Fluid

Liou Zhiyong, L. Qiang, Gang Yang, Zhang Fengyan, T. Ma
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引用次数: 5

Abstract

Wellbore instability caused by the dispersion of the clay is one of the most important challenges in drilling operation of fractured formations. The synthesis of new plugging inhibitors and the research of drilling fluid systems are key steps to keep the wellbore stabilization. In this paper, the limitations of conventional drilling fluid inhibitors are discussed and a new plugging inhibitor PAS-5 is synthesized by using amine inhibitor, polyethylene glycol and asbestos fiber as the main monomers. The detailed synthesis step of the plugging inhibitor PAS-5 is illustrated and its action mechanism is explained by scanning electron microscopy. In order to express the good effect of the PAS-5, a new evaluation system is used to indicate its plugging performance. At the same time, the plugging inhibitor PAS-5 was used on-site drilling operation in the Ordos Basin. The results of research show that the synthesis process of PAS-5 is simple and the effect of plugging inhibition is obvious. Compared with conventional treatment agents? PAS-5 outperforms sulfonated asphalt FT-1 and emulsified asphalt RHJ-3 in terms of plugging inhibition performance, with a plugging rate of 90.5% and roller recovery rate of 93.7%. It also has better temperature resistance, there is almost no change in viscosity and filtrate loss when the temperature rises from room temperature to 80°C. The field application results indicated that PAS-5 meets the requirements of drilling, that the reaming time of the trips of the wells is shortened considerably, that the ROP is improved, and that the hole enlargement rate is less than 6%. During the drilling process, PAS-5 can inhibit formation hydration and seal small cracks, thus maintaining the stability of the borehole. This study synthesized a novel plugging inhibitor PAS-5 and an evaluation system was adopted to reveal its plugging performance, and achieved good application effect in on-site drilling operations.
新型水基钻井液堵漏抑制剂PAS-5的合成与应用
粘土分散引起的井筒失稳是裂缝性地层钻井作业中最重要的挑战之一。新型堵漏抑制剂的合成和钻井液体系的研究是保持井筒稳定的关键步骤。本文讨论了常规钻井液抑制剂的局限性,以胺类抑制剂、聚乙二醇和石棉纤维为主要单体合成了一种新型堵漏抑制剂PAS-5。阐述了封堵抑制剂PAS-5的详细合成步骤,并用扫描电镜分析了其作用机理。为了表达PAS-5的良好效果,采用了一种新的评价体系来评价PAS-5的封堵性能。同时,在鄂尔多斯盆地进行了现场钻井作业,使用了堵漏抑制剂PAS-5。研究结果表明,PAS-5的合成工艺简单,阻堵效果明显。与常规治疗剂比较?PAS-5的阻堵性能优于磺化沥青FT-1和乳化沥青RHJ-3,阻堵率为90.5%,压辊回收率为93.7%。具有较好的耐温性,当温度从室温上升到80℃时,粘度和滤液损失几乎没有变化。现场应用结果表明,PAS-5满足钻井要求,井起下钻扩眼时间明显缩短,机械钻速提高,扩眼率小于6%。在钻井过程中,PAS-5可以抑制地层水化,密封小裂缝,从而保持井眼的稳定性。本研究合成了一种新型堵漏抑制剂PAS-5,并建立了封堵性能评价体系,在现场钻井作业中取得了良好的应用效果。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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