Maximizing Production by Perforating with Accurate Dynamic Underbalance Using Electric Coiled Tubing Offshore Egypt

Ahmed ElSayed Ghonim, Amr Zeinhom Elfarran, O. Okasha, E. Haridy, M. Koriesh, Aly ElBasyouni Mousa, Ahmed Gaber AbdelSabor
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Abstract

This paper represents a challenging rig-less intervention in highly deviated wells with heavy oil that has always been a challenge to conventional electric line (e-line) that is not a valid intervention technique due to its inherent limitations in these harsh environments. Electric Coiled Tubing (E-CT) was utilized not only to achieve safer deployment of the guns, but also to allow real-time operations on three wells which were inaccessible due to heavy oil content and restricted e-line accessibility. A case study is presented for a campaign performed using E-CT to convey the perforating string while pumping nitrogen (N2) to lift the well and achieve flowing under-balance to maximize perforation clean-up and minimize skin. Real-time readings from gamma ray, pressure and temperature sensors were used to accurately position the guns, generate the desired dynamic underbalance, and finally validate successful detonation based on pressure and temperature responses. This was achieved while N2 lifting and firing the guns to optimize the required under-balance value providing immediate feedback related to the production gain to determine the zonal contributions and maximize the economical production gains. Dynamic wellbore behavior software modeling was also used to predict the dynamic under-balance effect for maximizing perforation efficiency. Deployment of E-CT was very challenging in terms of operational execution but was extremely beneficial for the safety of the pipe during such operations. A total of 13 runs comprising of milling, tubing cleaning and drifting were performed to remove the accumulated scales inside the production tubing and to ensure full accessibility to target intervals. Coiled Tubing (CT) dynamic modeling software was utilized to simulate the N2 rate needed to achieve the target underbalance while maintaining safe perforating parameters for the CT while firing the guns. As a result of software simulations, one of the three wells was then recommended for an acid wash treatment which achieved very effective results. 15 perforation runs were performed on the three wells re-perforating a total of 188 ft of interval, resulting in a production increase of more than 300%. This was a significant improvement compared to the previous campaign carried out in 2017 where perforating in static conditions showed no increase in production without work-over rig intervention. E-CT intervention also eliminated the need for waiting on rig schedule and avoiding deferred production.
在埃及海上使用电动连续油管,通过精确动态欠平衡射孔实现产量最大化
本文介绍了一种具有挑战性的稠油大斜度井无钻机修井技术,该技术一直是传统电缆(e-line)的挑战,由于其在恶劣环境中的固有局限性,它不是一种有效的修井技术。使用电子连续油管(E-CT)不仅可以实现更安全的射孔枪部署,还可以在由于稠油含量和限制电缆可达性而无法进入的三口井进行实时作业。介绍了使用E-CT传输射孔管柱的案例研究,同时泵入氮气(N2)来提升井眼,实现欠平衡流动,以最大限度地清理射孔并减少结皮。伽马射线、压力和温度传感器的实时读数用于精确定位射孔枪,产生所需的动态欠平衡,最后根据压力和温度响应验证成功引爆。这是在N2举升和发射射孔枪时实现的,以优化所需的欠平衡值,提供与生产增益相关的即时反馈,以确定层位贡献并最大化经济生产收益。动态井筒行为软件建模还用于预测动态欠平衡效应,以最大限度地提高射孔效率。在作业执行方面,E-CT的部署非常具有挑战性,但在此类作业期间,它对管柱的安全性非常有益。共进行了13趟作业,包括磨铣、油管清洗和漂移,以清除生产油管内累积的结垢,并确保完全进入目标层段。利用连续油管(CT)动态建模软件模拟实现目标欠平衡所需的N2速率,同时在发射射孔枪时保持连续油管的安全射孔参数。根据软件模拟结果,三口井中的一口被推荐进行酸洗处理,取得了非常有效的效果。三口井共进行了15次射孔作业,共射孔188英尺,产量增加了300%以上。与2017年进行的上一次作业相比,这是一个显着的改进,当时在没有修井机干预的情况下,静态条件下的射孔没有增加产量。E-CT干预也消除了等待钻机进度的需要,避免了延迟生产。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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