OPERATIONAL ASSESSMENTS TO IMPROVE THE MONITORING OF PETROLEUM CATALYTIC HYDRODESULFURIZATION PROCESSING

M. Abreu, C. Abreu
{"title":"OPERATIONAL ASSESSMENTS TO IMPROVE THE MONITORING OF PETROLEUM CATALYTIC HYDRODESULFURIZATION PROCESSING","authors":"M. Abreu, C. Abreu","doi":"10.5419/bjpg2020-0001","DOIUrl":null,"url":null,"abstract":"The present research evaluates the operational status of hydrodesulphurization oil processing based on the monitoring of the feed oil filtration system. The system is identified as a prognostic module, designed to predict the remaining catalyst activity in the trickle bed reactor. The influence of the oil feeding flow rate of the process was evaluated with focus on the level of activity of the catalyst bed of the reactor affected by content of soluble and fine contaminants of fed oil. During an operation campaign (45 days) of the HDS unity (filter, reactor) variations of LHSV (0.5 – 1.5 h-1) and pressure differential in the filter (110 – 200 Mpa) reflected in the reactor, where the activity of the catalyst diminished from 60 % to 54.0 %. The predictions, extrapolated to 700 campaign days, indicated a catalyst deactivation of about 50%, allowing a conversion of sulfur compounds around 43% to be maintained.","PeriodicalId":9312,"journal":{"name":"Brazilian Journal of Petroleum and Gas","volume":"31 1","pages":"001-006"},"PeriodicalIF":0.0000,"publicationDate":"2020-05-06","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Brazilian Journal of Petroleum and Gas","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.5419/bjpg2020-0001","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

The present research evaluates the operational status of hydrodesulphurization oil processing based on the monitoring of the feed oil filtration system. The system is identified as a prognostic module, designed to predict the remaining catalyst activity in the trickle bed reactor. The influence of the oil feeding flow rate of the process was evaluated with focus on the level of activity of the catalyst bed of the reactor affected by content of soluble and fine contaminants of fed oil. During an operation campaign (45 days) of the HDS unity (filter, reactor) variations of LHSV (0.5 – 1.5 h-1) and pressure differential in the filter (110 – 200 Mpa) reflected in the reactor, where the activity of the catalyst diminished from 60 % to 54.0 %. The predictions, extrapolated to 700 campaign days, indicated a catalyst deactivation of about 50%, allowing a conversion of sulfur compounds around 43% to be maintained.
改进石油催化加氢脱硫过程的运行评价监测
本研究在对进料油过滤系统进行监测的基础上,对加氢脱硫油处理的运行状况进行了评价。该系统被确定为一个预测模块,用于预测滴流床反应器中剩余的催化剂活性。考察了进油流量对反应器催化剂床层活性的影响,重点考察了进油中可溶性污染物和细污染物含量对反应器床层活性的影响。在HDS系统(过滤器,反应器)运行期间(45天),LHSV (0.5 - 1.5 h-1)和过滤器压差(110 - 200 Mpa)的变化反映在反应器中,其中催化剂活性从60%下降到54.0%。根据700天的预测,催化剂失活率约为50%,硫化合物转化率维持在43%左右。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 求助全文
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术官方微信