Integrated Loss Control and Prevention Technologies for Complex Deep Wells Based on Precise MPD

Gang Wang, H. Fan, Wei Zhang, Yang Yang, Zili Han, Hongxuan Wu, Wanjun Li, Jiaying Li, T. Zhou, Haiqiu Zhou, Jitong Liu
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Abstract

M15 well contains complex intervals, where anticlinal structures developed from faults make long mudstone barriers full of cracks, which makes it hard to predict pore pressure. Loss is one of the most serious problems during drilling and cementing, while blow out accidents happen sometimes. Previous casing programs hardly adjust to all complex intervals and conventional LCMs (loss control materials) play few roles. As a result, designated targets used to be rarely reached. It is proved that low pressure intervals shall be isolated firmly and complex intervals as well as reservoirs should be developed in independent intervals, thus casing programs have been modified. 188 lab tests were finalized, including 180°C hot rolling, anti-contamination test, lubricity test and inhibition experiments, in order to develop a kind of organic salt mud system that has premium inhibition, plugging, lubricating, heat & salt resistance properties. Precise MPD (managed pressure drilling) techniques are recommended to achieve near-balance drilling operation, solving borehole instability problems to some extent. In the second interval the organic salt mud system is applied, while logging and casing running may be accomplished in one time. Besides, strings can be tripped out smoothly and high pressure brine productive zones are drilled safely. φ339.7mm casing joints are set at the depth of 3848m in the second interval and φ244.5mm casing joints are set at the depth of 5177m in the third interval, in order that deeper complex formation may be developed in a separate casing interval in which precise MPD is applied with LCMs while drilling and compound plugging agents. Therefore, downhole pressure is precisely controlled and large cracks are plugged statically on 28 occasions. Designated targets have been all reached and 20 oil & gas productive layers have been developed. Downhole complexities arising from loss and blowout have been solved in M15, where φ339.7mm casing was set at the deepest interval in CNPC overseas operation history, making a new record of safe drilling operation, borehole quality and cementing quality. More oil and gas productive zones have been discovered and all designated targets have been achieved. New drilling experience got from M15 has significant meanings in the development of similar blocks.
基于精密MPD的复杂深井综合防漏技术
M15井层段复杂,断层发育的背斜构造形成了充满裂缝的长泥岩屏障,使得孔隙压力难以预测。漏失是钻井固井过程中最严重的问题之一,井喷事故时有发生。以前的套管方案很难适应所有复杂的层段,传统的lcm(防漏失材料)几乎不起作用。因此,过去很少能达到指定的目标。实践证明,低压层段应牢固隔离,复杂层段和储层应独立开发,因此对套管方案进行了改进。为研制出一种具有优异的缓蚀、堵塞、润滑、耐热、耐盐性能的有机盐泥浆体系,完成了包括180℃热轧、抗污染、润滑、缓蚀试验在内的188项实验室试验。建议采用精确的控压钻井技术,实现近平衡钻井作业,在一定程度上解决井眼失稳问题。第二段采用有机盐泥浆体系,测井和下套管可一次完成。此外,管柱可以顺利下入,高压盐水生产区域可以安全钻进。在第二层段3848m处设置φ339.7mm的套管接头,在第三层段5177m处设置φ244.5mm的套管接头,以便在单独的套管段开发更深的复杂地层,并在钻井时使用精确MPD与lcm结合并使用复合堵漏剂。因此,井下压力被精确控制,大裂缝被静态封堵了28次。已全部达到指定目标,开发了20个油气生产层。M15井解决了井喷漏失带来的井下复杂问题,在中石油海外作业历史上最深的井段下入φ339.7mm套管,创造了安全钻井作业、井眼质量和固井质量的新纪录。已经发现了更多的油气产层,并且已经完成了所有指定的目标。M15获得的钻井新经验对类似区块的开发具有重要意义。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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