Development and First Application of an Ultra-Low Density Non-Aqueous Reservoir Drilling Fluid in the United Arab Emirates: A Viable Technical Solution to Drill Maximum Reservoir Contact Wells Across Depleted Reservoirs

R. Jeughale, K. Andrews, S. A. Al Ali, T. Toki, Hisaya Tanaka, Ryosuke Sato, J. Luzardo, G. Sarap, Saumit Chatterjee, Z. Meki
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Abstract

Drilling and completion operations in depleted reservoirs, are challenging due to narrow margin between pore and fracture pressures. Therefore, Ultra-Low Density Reservoir Drilling Fluid (RDF) with optimum parameters is required to drill these wells safely. Design and effective field application of a sound engineered fluid solution to fulfill these operational demands are described. Ultra-Low Density RDF NAF with minimal fluid invasion characteristics was developed after extensive lab testing, to cover the fluid density from 7.2 – 8.0 ppg. The fluid properties were optimized based on reservoir requirements and challenging bottom-hole conditions. The design criteria benchmarks and field application details are presented. Fluids were stress tested for drill solids, reservoir water and density increase contamination. Multi-segment collaboration and teamwork were key during job planning and on-site job execution, to achieve operational success. For the first time in UAE, a major Offshore Operator successfully applied an Ultra-Low Density RDF-NAF, which provided remarkable stability and performance. The fluid was tested in the lab with polymeric viscosifier alone and in combination with organophilic clay. In order to gain rheology during the initial mixing, about 3.0 ppb of organophilic clay were introduced to system along with the polymeric viscosifier. Later, all the new fluid batches were built with polymeric additives alone to achieve target properties. A total of 10,250 ft of 8 ½" horizontal section was drilled to section TD with record ROP compared to previous wells in the same field, with no fluids related complications. With limited support from the solid control equipment, the team managed to keep the density ranging from 7.5 ppg to 7.8 ppg at surface condition, using premixed dilution. Bridging was monitored through actual testing on location and successfully maintained the target PSD values throughout the section by splitting the flow on three shaker screen size combination. Due to non-operation related issues, hole was kept static for 20 days. After such long static time, 8 ½" drilling BHA was run to bottom smoothly precautionary breaking circulation every 5 stands. Finally, after successful logging operation, 6 5/8" LEL liner was set to TD and the well completed as planned. Success of this field application indicates that an Ultra-Low density fluid can be designed, run successfully and deliver exemplary performance. Lessons learned are compared with conceptual design for future optimization. Laboratory test results are presented, which formed the basis of a seamless planned field application.
超低密度非水油藏钻井液在阿拉伯联合酋长国的开发和首次应用:一种可行的技术解决方案,可在枯竭油藏上钻出最大油藏接触井
由于孔隙和破裂压力之间的边界很小,在衰竭油藏中进行钻井和完井作业具有挑战性。因此,为了保证这些井的安全钻井,需要使用具有最佳参数的超低密度油藏钻井液(RDF)。本文描述了一种良好的工程流体解决方案的设计和有效的现场应用,以满足这些操作要求。经过大量的实验室测试,开发出了具有最小流体侵入特性的超低密度RDF NAF,可覆盖7.2 - 8.0 ppg的流体密度。根据储层要求和具有挑战性的井底条件,对流体性质进行了优化。介绍了设计标准、基准和现场应用细节。对钻井液进行了钻井固体、油藏水和密度增加污染的压力测试。在作业计划和现场作业执行过程中,多部门协作和团队合作是取得运营成功的关键。在阿联酋,一家大型海上作业公司首次成功应用了超低密度RDF-NAF,提供了出色的稳定性和性能。在实验室中对该液体进行了单独使用聚合增粘剂和与亲有机粘土联合使用的测试。为了在初始混合过程中获得流变性,在加入聚合物增粘剂的同时,加入约3.0 ppb的亲有机粘土。后来,为了达到目标性能,所有新批次的流体都单独添加了聚合物添加剂。与同一油田的前几口井相比,共钻了10250英尺的8½英寸水平段,达到了创纪录的ROP,没有出现与流体相关的并发症。在固体控制设备的有限支持下,该团队使用预混稀释剂,成功地将表面条件下的密度保持在7.5至7.8 ppg之间。通过现场实际测试监测桥接,通过在三种筛分器尺寸组合上分离流体,成功地保持了整个段的目标PSD值。由于非操作相关问题,井眼保持静态20天。经过这么长的静置时间后,每隔5层就可以将8 - 1 / 2”钻井底部钻具组合顺利下至底部。最后,测井作业成功后,将6 5/8”LEL尾管下至TD,并按计划完井。该油田的成功应用表明,超低密度流体可以设计、成功运行,并提供卓越的性能。将吸取的经验教训与概念设计进行比较,以便将来进行优化。给出了实验室测试结果,为无缝规划的现场应用奠定了基础。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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