{"title":"PERFORMANCE OF INTEGRATED TWO STAGE ANOXIC-AEROBIC SEQUENCING BATCH REACTOR IN THE TREATMENT OF SEWAGE","authors":"M. I. A. Isma, R. Ashvini, M. Munira","doi":"10.31580/SPS.V1I2.649","DOIUrl":null,"url":null,"abstract":"A 10 L SBR reactor was operated on a two cycles per day with total cycle time of 500 minutes. This study explored the impact of a 300 minute react period with alternating two stage anoxic-aerobic phases starting at 120 minutes to 30 minutes on effluent quality, sludge settleability and particle size distribution.The overall removal efficiencies for COD, TSS and NH4-N were 93.8%, 98.4 % and 85.9%, respectively. The results indicated a good process performance with the first 2h anoxic/1.5 h aerobic period with removals of 66.0%, 78.5% and 59.4 % for COD, NH4-N and TSS removal respectively.The NH4-N removal was not enhanced although the anoxic period was lengthened by 1 h with low removal of 4.5 % and subsequent 7.2% of the second aerobic phase. There was an increase in the particle size of the sludge from 117.743μm to 127.310μm over an operating period of 35 days.","PeriodicalId":21574,"journal":{"name":"Science Proceedings Series","volume":"30 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2019-04-24","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Science Proceedings Series","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.31580/SPS.V1I2.649","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
A 10 L SBR reactor was operated on a two cycles per day with total cycle time of 500 minutes. This study explored the impact of a 300 minute react period with alternating two stage anoxic-aerobic phases starting at 120 minutes to 30 minutes on effluent quality, sludge settleability and particle size distribution.The overall removal efficiencies for COD, TSS and NH4-N were 93.8%, 98.4 % and 85.9%, respectively. The results indicated a good process performance with the first 2h anoxic/1.5 h aerobic period with removals of 66.0%, 78.5% and 59.4 % for COD, NH4-N and TSS removal respectively.The NH4-N removal was not enhanced although the anoxic period was lengthened by 1 h with low removal of 4.5 % and subsequent 7.2% of the second aerobic phase. There was an increase in the particle size of the sludge from 117.743μm to 127.310μm over an operating period of 35 days.