Remediation of Hydrate Plug in Gas Export Line – A West Africa Deep Water Case

F. Papot, Celma Alexandre, M. Abdulssalam, Ambrosio Chita, A. Pina, Antonio Chipoque, P. Glénat
{"title":"Remediation of Hydrate Plug in Gas Export Line – A West Africa Deep Water Case","authors":"F. Papot, Celma Alexandre, M. Abdulssalam, Ambrosio Chita, A. Pina, Antonio Chipoque, P. Glénat","doi":"10.4043/29946-ms","DOIUrl":null,"url":null,"abstract":"\n This paper describes a recent hydrate plug issue experienced in a 12inch gas export line of one of TOTAL E&P operated FPSOs in the deep water of West Africa. In summer 2018, due to long-term maintenance work on the dehydration unit of the FPSO's gas compression, the off- spec produced gas was injected into a remote subsea gas well injector to avoid gas flaring, in line with TOTAL's flaring policy. Methanol was continuously injected for hydrate inhibition. Unfortunately, at the end of the operation, a hydrate plug occurred in the 12-inch gas export line. Through a multi–disciplinary crisis management team, all necessary efforts and procedures were implemented to remove the plug from the line in less than 1 week. The main steps included topsides depressurisation, a subsea intervention, additional hydrate inhibitor injection (Methanol and especially MEG) and liquid flushing operations.","PeriodicalId":10927,"journal":{"name":"Day 3 Thu, October 31, 2019","volume":"27 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2019-10-28","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 3 Thu, October 31, 2019","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.4043/29946-ms","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0

Abstract

This paper describes a recent hydrate plug issue experienced in a 12inch gas export line of one of TOTAL E&P operated FPSOs in the deep water of West Africa. In summer 2018, due to long-term maintenance work on the dehydration unit of the FPSO's gas compression, the off- spec produced gas was injected into a remote subsea gas well injector to avoid gas flaring, in line with TOTAL's flaring policy. Methanol was continuously injected for hydrate inhibition. Unfortunately, at the end of the operation, a hydrate plug occurred in the 12-inch gas export line. Through a multi–disciplinary crisis management team, all necessary efforts and procedures were implemented to remove the plug from the line in less than 1 week. The main steps included topsides depressurisation, a subsea intervention, additional hydrate inhibitor injection (Methanol and especially MEG) and liquid flushing operations.
天然气输气管线水合物堵塞的修复——西非深水案例
本文描述了最近在西非深水区,道达尔勘探与开发公司的一艘fpso的12英寸天然气出口管线中遇到的水合物堵塞问题。2018年夏季,由于FPSO气体压缩脱水装置的长期维护工作,不合规格的产出气体被注入远程海底气井注入器,以避免天然气燃烧,符合道达尔的燃烧政策。连续注入甲醇进行水合物抑制。不幸的是,在作业结束时,在12英寸的天然气出口管道中发生了水合物堵塞。通过一个多学科的危机管理团队,采取了所有必要的努力和程序,在不到一周的时间内从管道上拆除了塞子。主要步骤包括上部减压、海底干预、额外的水合物抑制剂注入(甲醇,尤其是MEG)和液体冲洗作业。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
求助全文
约1分钟内获得全文 求助全文
来源期刊
自引率
0.00%
发文量
0
×
引用
GB/T 7714-2015
复制
MLA
复制
APA
复制
导出至
BibTeX EndNote RefMan NoteFirst NoteExpress
×
提示
您的信息不完整,为了账户安全,请先补充。
现在去补充
×
提示
您因"违规操作"
具体请查看互助需知
我知道了
×
提示
确定
请完成安全验证×
copy
已复制链接
快去分享给好友吧!
我知道了
右上角分享
点击右上角分享
0
联系我们:info@booksci.cn Book学术提供免费学术资源搜索服务,方便国内外学者检索中英文文献。致力于提供最便捷和优质的服务体验。 Copyright © 2023 布克学术 All rights reserved.
京ICP备2023020795号-1
ghs 京公网安备 11010802042870号
Book学术文献互助
Book学术文献互助群
群 号:481959085
Book学术官方微信