F. Papot, Celma Alexandre, M. Abdulssalam, Ambrosio Chita, A. Pina, Antonio Chipoque, P. Glénat
{"title":"Remediation of Hydrate Plug in Gas Export Line – A West Africa Deep Water Case","authors":"F. Papot, Celma Alexandre, M. Abdulssalam, Ambrosio Chita, A. Pina, Antonio Chipoque, P. Glénat","doi":"10.4043/29946-ms","DOIUrl":null,"url":null,"abstract":"\n This paper describes a recent hydrate plug issue experienced in a 12inch gas export line of one of TOTAL E&P operated FPSOs in the deep water of West Africa. In summer 2018, due to long-term maintenance work on the dehydration unit of the FPSO's gas compression, the off- spec produced gas was injected into a remote subsea gas well injector to avoid gas flaring, in line with TOTAL's flaring policy. Methanol was continuously injected for hydrate inhibition. Unfortunately, at the end of the operation, a hydrate plug occurred in the 12-inch gas export line. Through a multi–disciplinary crisis management team, all necessary efforts and procedures were implemented to remove the plug from the line in less than 1 week. The main steps included topsides depressurisation, a subsea intervention, additional hydrate inhibitor injection (Methanol and especially MEG) and liquid flushing operations.","PeriodicalId":10927,"journal":{"name":"Day 3 Thu, October 31, 2019","volume":"27 1","pages":""},"PeriodicalIF":0.0000,"publicationDate":"2019-10-28","publicationTypes":"Journal Article","fieldsOfStudy":null,"isOpenAccess":false,"openAccessPdf":"","citationCount":"0","resultStr":null,"platform":"Semanticscholar","paperid":null,"PeriodicalName":"Day 3 Thu, October 31, 2019","FirstCategoryId":"1085","ListUrlMain":"https://doi.org/10.4043/29946-ms","RegionNum":0,"RegionCategory":null,"ArticlePicture":[],"TitleCN":null,"AbstractTextCN":null,"PMCID":null,"EPubDate":"","PubModel":"","JCR":"","JCRName":"","Score":null,"Total":0}
引用次数: 0
Abstract
This paper describes a recent hydrate plug issue experienced in a 12inch gas export line of one of TOTAL E&P operated FPSOs in the deep water of West Africa. In summer 2018, due to long-term maintenance work on the dehydration unit of the FPSO's gas compression, the off- spec produced gas was injected into a remote subsea gas well injector to avoid gas flaring, in line with TOTAL's flaring policy. Methanol was continuously injected for hydrate inhibition. Unfortunately, at the end of the operation, a hydrate plug occurred in the 12-inch gas export line. Through a multi–disciplinary crisis management team, all necessary efforts and procedures were implemented to remove the plug from the line in less than 1 week. The main steps included topsides depressurisation, a subsea intervention, additional hydrate inhibitor injection (Methanol and especially MEG) and liquid flushing operations.