Case study on the failure analysis of turbojet compressor blades

Jéssica Silva Rocha Pinho, L. Campanelli, D. Reis
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引用次数: 2

Abstract

With a turbojet compressor that had its blades fractured during laboratory tests, this work carried out a failure analysis aiming at characterizing the problem, identifying the fracture mechanism and proposing a potential post-manufacturing improvement. Typical steps of a failure analysis were performed, including visual and fractographic analyzes via stereomicroscopy and scanning electron microscopy. The evidence indicated that the component failed due to fatigue, with the presence of very evident striations on the fracture surface, due to a high surface roughness. Therefore, it was considered suitable to propose a shot peening treatment on the product as a way of inducing residual compressive stresses and hindering the process of nucleation of a fatigue crack.
涡喷发动机压气机叶片失效分析实例研究
针对一台涡轮喷气压气机的叶片在实验室测试中出现断裂的情况,本研究开展了故障分析,旨在对问题进行表征,确定断裂机理,并提出潜在的制造后改进措施。进行了典型的失效分析步骤,包括通过立体显微镜和扫描电子显微镜进行视觉和断口分析。证据表明,由于高表面粗糙度,该部件由于疲劳而失效,在断口表面存在非常明显的条纹。因此,建议对产品进行喷丸强化处理,作为诱导残余压应力和阻止疲劳裂纹形核过程的一种方法。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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12 weeks
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