Grooving corrosion of seam welded oil pipelines

Mohamed Hanafy El-Sayed
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引用次数: 6

Abstract

24” pipeline carrying oil was failed in the form of longitudinal crack at the 6 O’clock position resulting in oil spill. The failed pipe was investigated to reveal the main cause of its failure. The procedure of investigation was built on studying the intact pipe, rupture area, parent material, and intact weld. Results of chemical analysis, mechanical properties, and microstructure of the pipe material were confirmed with the specified standard. Cracks were originated from weld defected sites, initiated by grooving corrosion, propagated by inertia at the normal designed pressure condition, and stopped when stress relief is attained. It is recommended to use high quality ERW pipe, with its seam weld line positioned around the 12 O’clock during installation, to minimize and decelerate grooving corrosion. It is also important to perform regular or routine inspection, on suitable intervals, determined by past experience.

缝焊输油管道的开槽腐蚀
24”输油管道在6点钟位置出现纵裂,导致原油泄漏。对失效管道进行了调查,找出了失效的主要原因。调查程序建立在研究完整管道、破裂区域、母材和完整焊缝的基础上。材料的化学分析、力学性能和显微组织均符合规定的标准。裂纹起源于焊缝缺陷部位,由沟槽腐蚀引起,在正常设计压力条件下由惯性传播,并在达到应力消除时停止。建议使用优质的ERW管,安装时焊缝线定位在12点钟左右,以减少和减缓槽腐蚀。根据过去的经验,在适当的时间间隔内进行定期或例行检查也很重要。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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