Failure investigation of a secondary super heater tube in a 140 MW thermal power plant

Atanu Saha, H. Roy
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引用次数: 22

Abstract

This article describes the findings of a detailed investigation into the failure of a secondary super heater tube in a 140 MW thermal power plant. Preliminary macroscopic examinations along with visual examination, dimensional measurement and chemical analysis were carried out to deduce the probable cause of failure. In addition optical microscopy was a necessary supplement to understand the cause of failure. It was concluded that the tube had failed due to severe creep damage caused by high metal temperature during service. The probable causes of high metal temperature may be in sufficient flow of steam due to partial blockage, presence of thick oxide scale on ID surface, high flue gas temperature etc. rupture.

某140mw火电厂二次过热加热器管失效分析
本文介绍了对某140mw火电厂二次过热加热器管失效的详细调查结果。通过初步的宏观检查、目视检查、尺寸测量和化学分析,推断出可能的失效原因。此外,光学显微镜是了解失败原因的必要补充。结果表明,由于使用过程中金属温度过高,造成了严重的蠕变损伤,导致钢管失效。金属温度高的可能原因可能是由于部分堵塞导致蒸汽流量不足,ID表面存在厚氧化垢,烟气温度高等破裂。
本文章由计算机程序翻译,如有差异,请以英文原文为准。
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